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34-115-23754

Well Details

Well ID: 34-115-23754
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County: Morgan
Municipality:
Operator Name: ARTEX OIL COMPANY
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 1985-03-08
Unconventional: No
Configuration: Vertical
Well Status: Producing
Violations: 0
Latitude: 39.7055904
Longitude: -81.66755014

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
1986-0 31076.0 640.0
1987-0 15862.0 241.0
1988-0 16944.0 233.0
1989-0 13779.0 149.0
1990-0 11051.0 72.0
1991-0 9233.0 70.0
1993-0 8271.0 0.0
1994-0 9353.0 65.0
1995-0 8701.0 80.0
1996-0 7899.0 0.0
1997-0 6634.0 0.0
1998-0 6087.0 69.0
2000-0 4092.0 0.0
2001-0 6096.0 0.0
2002-0 4296.0 0.0
2003-0 6493.0 55.0
2004-0 4951.0 0.0
2005-0 4615.0 0.0
2006-0 4685.0 0.0
2007-0 4366.0 68.0
2008-0 3662.0 0.0
2009-0 3699.0 0.0
2010-0 2826.0 0.0
2011-0 2908.0 0.0
2012-0 3580.0 0.0
2013-0 3584.0 0.0
2014-0 3680.0 365.0 0.0 365.0

For data sources see[1]

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
1125152110 2005-08-22 No violations noted,A.D. not being used and well is equipped with 1-100 bbl storage tank. Compliance Notice
1205590300 2008-03-11 A.D. not being used,well is equipped with tubing(rabbit well) and 1-100 bbl tank with dike in place.
1362157370 2013-03-01 Well is not hooked up for annular disposal, but is currently in production. Well is equipped with an artificial lift pump(rabbit pump). The top of the 8 casing is level with the ground and appears to have a leak as witnessed by the bubbling of gas from its side. There was a slight odor of gas. There is one 100 barrel tank and separator up by the road, and there is a chart in the meter. The identification is in poor condition. I talked with the well tender Bobby Fritz and he said he would be out to take a look at the well but would not be able to do anything until drier weather. He said he would also take care of the ID issues. 03/06/2013: Bobby called and stated they repaired the leak.
1363198584 2013-03-13 Well is in compliance.
PL9447 Preliminary Restoration done information from Data Point

For data sources see[2]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20. 
  2. "Ohio Department of Natural Resources RBDMS". [2]. 2015-06-19. Retrieved 2015-06-20.