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34-153-21073

Well Details

Well ID: 34-153-21073
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County: Summit
Municipality:
Operator Name: MAVERICK OIL & GAS INC
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 1982-12-06
Unconventional: No
Configuration: Vertical
Well Status: Plugged and Abandoned
Violations: 0
Latitude: 41.03629363
Longitude: -81.60300237

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
1984-0 6132.0 260.0
1985-0 5274.0 535.0
1986-0 1965.0 825.0
1987-0 1965.0 825.0
1988-0 1295.0 603.0
1989-0 785.0 632.0
1990-0 837.0 491.0
1991-0 635.0 136.0
1993-0 32.0 210.0
1994-0 0.0 0.0
1995-0 0.0 0.0
1996-0 0.0 0.0
1997-0 0.0 0.0
1998-0 0.0 0.0
1999-0 0.0 0.0
2000-0 72.0 0.0
2001-0 348.0 22.0
2002-0 7.0 22.0
2005-0 442.0 0.0

For data sources see[1]

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
-415657859 2004-11-04 Status check inspection - no violations at this time.
417146378 2013-04-27 This well is not plugged but a plugging report was filed by the Operator using the wrong API number. I inspected this well on 4/27/2013. The last reported production was listed as 2005. Bob Worstall last inspected this well on 8/19/2005 and no corrective measures have taken place. I found the tank battery to consist of 1- 210 Bbl. Stock tank, 1- 30 Bbl. Plastic brine tank , 1- 2408 Separator with Gas Measurement Meter ( old chart ). No leaks were observed at the tank battery at this inspection. The well consisted of a Pumping Jack ( Model 40 ) and associated valving and plumbing. No leaks were observed at the wellhead during this inspection. The pump jack was missing an electric motor and thus inoperative. Domestic gas equipment was present but not utilized. Both areas were fenced and locked.
-512611277 2005-08-19 A contractor for the City of Barberton, while installing fence posts, severed the plastic flowline for this well. No liquids were released.

For data sources see[2]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20. 
  2. "Ohio Department of Natural Resources RBDMS". [2]. 2015-06-19. Retrieved 2015-06-20.