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Well ID: 34-121-23393 | Loading map...
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County: Noble | |
Municipality: | |
Operator Name: ARTEX OIL COMPANY | |
Well Pad ID: | |
Farm/Lease Name: | |
First Permit Date: | |
Last Permit Date: | |
Spud Date: 1984-12-31 | |
Unconventional: No | |
Configuration: Vertical | |
Well Status: Producing | |
Violations: 0 | |
Latitude: 39.63846758 | |
Longitude: -81.55972289 |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
---|---|---|---|---|---|---|
1993-0 | 2802.0 | 0.0 | ||||
1994-0 | 2229.0 | 0.0 | ||||
1995-0 | 2539.0 | 0.0 | ||||
1996-0 | 1881.0 | 0.0 | ||||
1997-0 | 1738.0 | 0.0 | ||||
1998-0 | 1071.0 | 0.0 | ||||
1999-0 | 1189.0 | 0.0 | ||||
2000-0 | 1173.0 | 0.0 | ||||
2001-0 | 2740.0 | 0.0 | ||||
2002-0 | 0.0 | 0.0 | ||||
2003-0 | 0.0 | 0.0 | ||||
2004-0 | 536.0 | 171.0 | ||||
2005-0 | 610.0 | 159.0 | ||||
2006-0 | 894.0 | 87.0 | ||||
2007-0 | 1102.0 | 0.0 | ||||
2008-0 | 1206.0 | 160.0 | ||||
2009-0 | 563.0 | 99.0 | ||||
2010-0 | 229.0 | 72.0 | ||||
2011-0 | 390.0 | 0.0 | ||||
2012-0 | 390.0 | 119.0 | ||||
2013-0 | 395.0 | 92.0 | ||||
2014-0 | 213.0 | 365.0 | 0.0 | 365.0 |
For data sources see[1]
INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID | VIOLATION CODE | VIOLATION COMMENT |
---|---|---|---|---|---|---|
1077363710 | 2004-02-20 | On location to witness plugging operation .Rabbit was stuck in tubing decision was made to pull tubing out of hole to free rabbit attempted to run tubing back in hole to set bottom plug unable to do so due to 4.5 casing being parted or rotted out.Tried to run 4 mandrel in hole to open up casing unable to get past2990' due to cavings decision was made to attempt to wash out cavings2-23-04.Company rep called and stated they ran approximatly 2200' of new 4.5 casing back in hole. | ||||
PL7439 | Preliminary Restoration done information from Data Point |
For data sources see[2]