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34-155-23772

Well Details

Well ID: 34-155-23772
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County: Trumbull
Municipality:
Operator Name: KLEESE DEVELOPMENT ASSOCS
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 2004-11-29
Unconventional: No
Configuration: Vertical
Well Status: Producing
Violations: 0
Latitude: 41.21933273
Longitude: -80.76092761

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
2006-0 5263.0 63.0
2007-0 5073.0 44.0
2008-0 4730.0 153.0
2010-0 3607.0 143.0
2011-0 2934.0 0.0
2012-0 2618.0 44.0
2013-0 2329.0 53.0
2014-0 2054.0 365.0 0.0 365.0

For data sources see[1]

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
1202360419 2006-05-11 Case# 06-004 , Regis Patrick . Inspection of well showed no violations . There is a sales line locacted across street from complaintant's home approx. 60' . The gas meter showed it is on a 12 hour timer . I advised Regis and his wife the sound they hea
1342203139 2012-07-13 On 7/13/2012, I completed a preliminary restoration well inspection status check. My inspection found the well was a plunger lift unit (rabbit) that was in good condition. The tank battery contained one 100 barrel oil storage tank with the proper identification posted, one 50 barrel brine tank, and a separator, I notice no visible spills or leaks. The lease road was in good condition, there are no violations at this time.
1347542841 2012-07-13 I completed a production inspection status check. My inspection found the well equipped with a plunger lift unit (rabbit) that was in good condition. The tank battery contained one 100 barrel oil storage tank, one 50 barrel brine storage tank, a separator, and the proper identification. I noticed no visible spills or leaks. The lease road was in good condition. There are no violations at this time.
-1518196804 2014-12-15 I was on location for a status check. During my inspection, I found the well in production. The well was equipped with a plunger lift assembly. The tank battery consisted of a 100 barrel production tank, a 50 barrel brine tank and separator. A dike surrounded the production equipment. A bull plug was installed on the load line. An identification sign was properly posted. The lease road was in stable condition. The well was placed into production prior to House Bill 278.
1696023416 2004-11-30 Rose Run drilling co. . No violations .
-378234955 2004-12-03 Rig drilling at 4122' .

For data sources see[2]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20. 
  2. "Ohio Department of Natural Resources RBDMS". [2]. 2015-06-19. Retrieved 2015-06-20.