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34-155-22621

Well Details

Well ID: 34-155-22621
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County: Trumbull
Municipality:
Operator Name: OHIO VALLEY ENERGY SYSTEM CORP
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 1984-10-15
Unconventional: No
Configuration: Vertical
Well Status: Producing
Violations: 0
Latitude: 41.21382225
Longitude: -80.87994364

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
1985-0 6063.0 332.0
1986-0 13164.0 282.0
1987-0 8629.0 198.0
1988-0 13444.0 528.0
1989-0 9407.0 352.0
1990-0 21603.0 530.0
1991-0 15434.0 462.0
1992-0 12826.0 300.0
1993-0 10472.0 180.0
1994-0 8964.0 147.0
1995-0 7015.0 144.0
1996-0 1542.0 0.0
1997-0 7843.0 109.0
1998-0 8210.0 130.0
1999-0 6838.0 88.0
2000-0 6660.0 145.0
2001-0 5251.0 96.0
2002-0 1312.0 65.0
2003-0 4585.0 36.0
2004-0 5281.0 93.0
2005-0 4757.0 121.0
2006-0 4795.0 73.0
2007-0 4290.0 28.0
2008-0 4778.0 60.0
2013-0 2731.0 38.0
2014-0 4205.0 365.0 101.0 365.0

For data sources see[1]

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
1375273800 2013-07-17 My inspection found the well in production. The well was equipped with a plunger lift unit. I noticed a flow line leak approximately 15' northeast of the wellhead in a 10' x 3' water puddle. The tank battery contained a 100 barrel production tank, a 50 barrel brine tank, and a separator. The dike was weathered and not capable of meeting containment requirements. There was a plug on the load line. Identification signs were posted on the production tank and well. There was a 7 day production chart at the separator. The lease road was in good condition. I called Don Nething at 330-283-5758. I instructed him to send the well tender to isolate the leak and make repair to the flow line. Also, I told him to build a new dike capable of meeting containment requirements.
-1751297846 2013-07-30 My inspection found the flow line leak repaired per my request.
PL3690 Preliminary Restoration done information from Data Point

For data sources see[2]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20. 
  2. "Ohio Department of Natural Resources RBDMS". [2]. 2015-06-19. Retrieved 2015-06-20.