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Well ID: 34-035-22068 | Loading map...
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County: Cuyahoga | |
Municipality: | |
Operator Name: BASS ENERGY CO INC | |
Well Pad ID: | |
Farm/Lease Name: | |
First Permit Date: | |
Last Permit Date: | |
Spud Date: 2009-03-22 | |
Unconventional: No | |
Configuration: Vertical | |
Well Status: Producing | |
Violations: 0 | |
Latitude: 41.52286319 | |
Longitude: -81.44021727 |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
---|---|---|---|---|---|---|
2009-0 | 30957.0 | 95.0 | ||||
2010-0 | 67628.0 | 84.0 | ||||
2011-0 | 36117.0 | 0.0 | ||||
2012-0 | 26002.0 | 31.0 | ||||
2013-0 | 17649.0 | 42.0 | ||||
2014-0 | 15644.0 | 365.0 | 0.0 | 365.0 |
For data sources see[1]
INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID | VIOLATION CODE | VIOLATION COMMENT |
---|---|---|---|---|---|---|
1001900923 | 2012-09-26 | The unit consists of a 2-tank battery (TB) with mechanical separator with plunger-lift at wellhead. The unit has a 8-foot fence enclosure at the TB and wellhead which are locked. The spacing is in accordance with the rule, and the valving and mechanicals are in good repair. I did not observe any signs of leaking product or gas vapors. The tank battery dike is adequate. The unit ID is good. No violations noted. | Compliance Notice | |||
-1194136310 | 2009-10-29 | |||||
1231115233 | 2009-04-02 | pits being closed | ||||
1247669559 | 2009-07-08 | Received phone call from company reporting gas leaking from well head. Responded to site and arrived approximately 2:45pm. The Company had the leak fixed and was doing corrective measures for cleaning up of the oil sprayed area to the south of the well. Which consists of the driveway (15'X15')and yard (15'X20').EPA (Bart Ray) told company to remove the soil off site. PeatSorb was applied to remediate the drive. Site was contained the same day. Total oil loss 15-20 gallons. EPA also advised company to put booms around sewer drains. NO OIL GOT INTO SEWERS. | ||||
1247672460 | 2009-07-09 | The oil was cleaned up around the wellhead and well site .Tempory fence was installed. The 2 tubing was repaired at the well head. Area will be graded and seeded. Permanent fence will be installed in 2 weeks. | ||||
-1411629276 | 2008-11-18 | trees cut site being worke on | ||||
-1419674349 | 2009-12-04 | no violation at time of inspection. | ||||
165997854 | 2009-04-27 | company working on getting well perforated. | ||||
2020453398 | 2009-12-04 | |||||
204981198 | 2009-03-26 | drilling at 2150' 4.5 possible on Sunday | ||||
-2141763771 | 2009-07-20 | The grassy area to the south of paved drive way was sprayed by oil.The soil was removed and replaced ,this area was seeded and starwed. | ||||
495787386 | 2015-02-20 | I inspected this well as part of routine inspection activity. The wellhead mechanical plunger lift and tank battery enclosures are locked and secure. System fittings and connections are secure and free from signs of leakage or problems. Load-outs are plugged, locked and secure. ID signage is present and accurate. Access to the unit is shared with the adjacent apartment community. At the time of this inspection, there is 12 to 14 inches of snow cover which obscures some surficial features. | ||||
-980031506 | 2009-09-23 |
For data sources see[2]