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34-073-23405

Well Details

Well ID: 34-073-23405
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County: Hocking
Municipality:
Operator Name: JEANIE ENTERPISES LLC
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 1994-08-17
Unconventional: No
Configuration: Vertical
Well Status: Producing
Violations: 0
Latitude: 39.56582589
Longitude: -82.44674208

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
1995-0 11329.0 0.0
1996-0 0.0 0.0
1997-0 4157.0 0.0
1998-0 6358.0 0.0
1999-0 3024.0 0.0
2000-0 452.0 0.0
2001-0 0.0 0.0
2002-0 0.0 0.0
2003-0 0.0 0.0
2004-0 0.0 0.0
2005-0 508.0 0.0
2006-0 0.0 0.0
2007-0 2007.0 0.0
2008-0 201.0 0.0
2009-0 870.0 0.0
2010-0 0.0 0.0
2011-0 0.0 0.0
2012-0 1409.0 0.0
2013-0 0.0 0.0
2014-0 0.0 365.0 0.0 365.0

For data sources see[1]

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
-1024541674 2003-02-07 Preliminary Rest meets 1509.072(A) requirements Compliance Notice
-1024541674 2003-02-07 Preliminary Rest meets 1509.072(A) requirements Compliance Notice
-1024541674 2003-02-07 Preliminary Rest meets 1509.072(A) requirements Phone Call
1114192479 2009-08-17 A follow-up inspection revealed non-compliance.
121866358 2012-04-16 Upon inspection there was evidence of a small spill which had been cleaned up. There was one leaky connection on a flow line that ran from the well to the separator. Mr. Danny Baker was notified of this. He is still currently working on the well. He stated that there are still some plumbing issues due to salt.
1223041119 2008-09-18 A follow-up inspection revealed that the steel line from this well has not been buried below ground. Valves are closed and the well is shut-in at this time.. Contamination and pollution surrounding the tank has been cleaned up.
1223304649 2008-09-23 A follow-up inspection revealed that work is being performed on burying the steel flowline. The pumper for this company states that they will bury the line and also bring in topsoil to ensure cover for a few sections.
-1267180093 2011-11-10 Checked on status of previous flow line leak. Area had been remediated, and flow line buried.
1269i11651156 2001-03-27 Ad check for Columbus , Ad not in use.
1269i95 2000-10-25 Follow - up on NOV , In - Compliance , all violations corrected.
1302724931 2011-03-31 Received call from Walter Born who is the caretaker of the Brandt farm. He stated that the motor on the pumpjack had been removed. This was verified in the field. With the exception of the missing motor, the well was equipped for production. Spoke with pumper about it and he stated that the motor went bad and there are broken rods in the well. He said that he will get it back into production soon but mainly for gas. Production reports for 2009 showed 870 mcf of gas produced. For 2010 it showed 818 bbl of brine.
-1432323213 2008-06-27 A complaint was received by the DMRM requesting that an above ground flowline to be buried. An inspection revealed that several section of this flowline located in field will need to be buried. Dead vegetation observed outside the dike. Hay observed around section of the dike covering contaminated soil. The soil will need to be removed. Identification will also be required.
-1465832049 2011-11-04 Received call from Walter Borne, caretaker of the Brandt Farm, at 12:31 pm alleging a flow line leak that was spewing brine. I arrived on site at 12:57 pm. Upon inspection I found an area of impact with a 25 foot radius caused by a small hole in a 2 inch flow line. It sprayed 10 feet into the air and the wind blew it over the ground. A sample of the water was tested with a high range Quantab. It maxed the test strip out. There was 5 or 6 gallons of brine pooled on the ground. There was also a T with a 2 inch valve without a plug in close proximity to the leak. A call was made to Joe Scmelzer and a voicemail was left explaining the situation. Danny Baker responded at 1:12 pm, and met me at the site. I explained to him that the leak must be fixed that day, and the remediation of the area must be done by next week. He agreed. Site was inspected again on 11/10/11 and site had been cleaned up complete with seed and straw.
162798605 2009-07-16 A follow-up inspection revealed non-compliance. An inspection conducted on 4/21/2009 revealed that separator has been placed 10' from the well. The lease road is eroding and will require grading. Move separator to location 50' from the well. Grade lease road.
170406315 2009-10-20 A follow-up inspection revealed non-compliance. No action has been taken by company to resolve violations.
1919142902 2010-04-22 A follow-up inspection revealed compliance.
-1987055716 2005-12-15 Checked AD for Columbus, AD not being used.
1989210298 2008-10-14 A follow-up inspection revealed compliance.
2094465015 2009-10-01 An inspection revealed non-compliance. No action taken to comply with violations. The lease road contains approx 6 to 1' ruts at midsection to top locations. The landowner has placed hay bales and vegetative debris in an attempt to prevent further erosion. The lease road overall length approx 500' over hillside, which had also been utilized to access Permit No. 2073. The well owner, Ms. Jeanie Schmelzer had been previously contacted by telephone. She stated that they would need more time and agreed to 10/1/2009 extension of NOV. Ms. Schmelzer was asked if this time frame was sufficient. She reassured me that they could meet this deadline.
-453213535 2009-10-30 A follow-up inspection revealed non-compliance. No action to comply with violations. At time of inspection, collapsable nylon line and corrugated line not connected to well. Pump observed next to creek with attached line and filter placed in creek.
555266131 2008-09-29 A follow-up inspection revealed non-compliance. It was noted that the company has dug a trench for the placement of the steel line. More work will need to be performed.
-674014415 2009-08-26 A follow-up inspection revealed non-compliance.
816438013 2009-05-19 A follow-up inspection revealed non-compliance. The well was observed pumping at time of the inspection.
-985900571 2009-04-21 A complaint was received alleging line burial and erosion from lease road. An inspection revealed that approximately 300' of the lease road would need to be addressed, due to erosion. The lease road contains ruts and washing out down below into pasture field near creek. The road had been utilized during the plugging process of Permit No. 2073 and the well owner had been aware that the lease road would need to be repaired. Note: The location contains a spring. The company has equipment placed on location to perform dirt work. Plastic flowline was observed to have now been placed over a steep hill and routed to a separator located approximately 10' from the well. Mr. Danny Baker with Jeanie Enterprises was contacted by telephone regarding the complaint and inspection. Mr. Baker states that the flowline would be re-routed and buried along the lease road when it has been repaired. Water bars were recommended to Mr. Baker to be placed along the lease road. Mr. Baker was also instructed to move the separator (recently installed) to a location 50' from the well.

For data sources see[2]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20. 
  2. "Ohio Department of Natural Resources RBDMS". [2]. 2015-06-19. Retrieved 2015-06-20.