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Well ID: 34-129-20236 | Loading map...
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County: Pickaway | |
Municipality: | |
Operator Name: HOUGHTON INVESTMENTS, L.L.C. | |
Well Pad ID: | |
Farm/Lease Name: | |
First Permit Date: | |
Last Permit Date: | |
Spud Date: 2011-10-06 | |
Unconventional: No | |
Configuration: Vertical | |
Well Status: Final Restoration | |
Violations: 0 | |
Latitude: 39.55931406 | |
Longitude: -83.07680452 |
INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID | VIOLATION CODE | VIOLATION COMMENT |
---|---|---|---|---|---|---|
1320082981 | 2011-10-15 | - On site for plugging well, dry hole
- Total depth 2390 Logger depth 2402 - 78 drill pipe ran back into well to 2390, set 1st plug and pull 18 joints of pipe. Pump gel and set 2nd plug and pull 37 joints of pipe. Set 3rd plug at bottom of surface casi |
||||
1328624407 | 2012-02-02 | - Pits filled in area graded, landowner has plowed agricultural farm field.
- Will approve final restoration. |
||||
989207434 | 2011-10-13 | - on site for surface casing. 8.750 Hole drilled to 620 feet, new 7 casing 20 Lbs. set to 605' Good circulation when cement was pump down. Formation Cementing did cement job. |
For data sources see[1]