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Well ID: 34-019-22567 | Loading map...
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County: Carroll | |
Municipality: | |
Operator Name: CHESAPEAKE EXPLORATION LLC | |
Well Pad ID: | |
Farm/Lease Name: | |
First Permit Date: | |
Last Permit Date: | |
Spud Date: 2014-03-31 | |
Unconventional: | |
Configuration: | |
Well Status: Producing | |
Violations: 0 | |
Latitude: 40.4957183 | |
Longitude: -81.05970938 |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
---|---|---|---|---|---|---|
2015-1 | 195459.0 | 66.0 | 13408.0 | 66.0 |
For data sources see[1]
INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID | VIOLATION CODE | VIOLATION COMMENT |
---|---|---|---|---|---|---|
2045686186 | 2015-01-28 | I inspected this well on 1/28/2015. The well was turned into production on 1/27/2015. Chesapeake Exploration's company , Mark Tribadeux, indicated the initial flowing of the well was without incident. The flowing pressure of the casing was 3505 psi. with the tubing flowing at 2835 psi.. The well was flowing through a 16/64th choke manifold with volumes estimated at 3 mmcfg/d and 10 - 15 barrels of oil and 10 - 15 barrels of frac load. The 13.375 annular pressure gauge read 0 psi. The 9.625 annular pressure gauge had a reading of 200 psi. This anomaly will be addressed by relieving the annular pressure and see if there is a reoccurrence. The proper signage was placed at the wellhead. Tank battery, heater treaters and compressor staions spacing was in compliance. |
For data sources see[2]