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Well ID: 34-163-20496 | Loading map...
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County: Vinton | |
Municipality: | |
Operator Name: BAY STATE EXPLORATION CO | |
Well Pad ID: | |
Farm/Lease Name: | |
First Permit Date: | |
Last Permit Date: | |
Spud Date: 1981-06-14 | |
Unconventional: No | |
Configuration: Vertical | |
Well Status: Producing | |
Violations: 0 | |
Latitude: 39.29434148 | |
Longitude: -82.58857593 |
INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID | VIOLATION CODE | VIOLATION COMMENT |
---|---|---|---|---|---|---|
-1089047842 | 2008-07-03 | The Division of Mineral Resources Management received information that Mr. Larry Horn has been removing equipment from Bay State Exploration wells. An inspection revealed that the well is idle. This well does not contain production equipment. Records indicate no production. Tubing was observed in the well bore. A Notice of Violation will be sent to Mr. Horn. | Compliance Notice | |||
228756092 | 2008-11-18 | A follow-up inspection revealed non-compliance. No action has been taken to resolve the violations. Valves remain closed on casing and tubing. No flowline was observed connected to the well. Note: Winter conditions at time of the inspection to include snow. New photographs obtained from this inspection. |
For data sources see[1]