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34-121-21978

Well Details

Well ID: 34-121-21978
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County: Noble
Municipality:
Operator Name: ATLAS NOBLE LLC
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 1977-08-18
Unconventional: No
Configuration: Vertical
Well Status: Plugged and Abandoned
Violations: 0
Latitude: 39.87136761
Longitude: -81.49643611

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
1984-0 2338.0 287.0
1985-0 1825.0 269.0
1986-0 1888.0 336.0
1987-0 1978.0 160.0
1988-0 1524.0 244.0
1989-0 699.0 149.0
1990-0 1302.0 207.0
1991-0 1983.0 359.0
1992-0 1781.0 233.0
1993-0 1809.0 227.0
1994-0 1982.0 167.0
1995-0 2074.0 258.0
1996-0 354.0 110.0
1997-0 921.0 171.0
1998-0 571.0 183.0
1999-0 1001.0 166.0
2000-0 902.0 83.0
2001-0 651.0 292.0
2002-0 1097.0 191.0
2003-0 1218.0 157.0
2004-0 789.0 172.0
2005-0 912.0 183.0
2006-0 1042.0 131.0
2007-0 95.0 0.0
2008-0 0.0 0.0
2009-0 0.0 0.0
2010-0 0.0 0.0
2011-0 0.0 0.0
2012-0 0.0 0.0
2013-0 0.0 25.0

For data sources see[1]

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
1366066194 2013-04-15 Well has been plugged resolving previous notice issued on 2/3/12.
1420233896 2012-02-03 Upon receiving request from landowner to inspect well site found well to be idle and last production reported on well was back in 2007,and well is equipped with 1-210 barrel tank with incomplete identification information and seperator with no chart in meter box and at wellhead there is 8.625 and 4.5 and 2.375 tubing and valves were closed on the day of my inspection,and after calling company rep stating that production casing has possible hole in it that is why well quit producing.

PLUG WELL OR REPAIR CASING AND PUT BACK INTO PRODUCTION. Failure to comply may result in bond forfieture.

-1464532135 2013-04-12 I am onsite to witness the placement of the bottom plug. A 30sk class A cement plug was placed at 5572' to 5179' through 2.375 tubing.
-1684566289 2013-04-11 My inspection today finds the well is being plugged by Nicks Plugging. An attempt to pump through the tubing failed and the rig crew started to trip the 2.375 tunbing.
855137577 2012-02-03 FOLLOW UP TO NOV # 1420233896 Upon receiving request from landowner to inspect well site found well to be idle and last production reported on well was back in 2007,and well is equipped with 1-210 barrel tank with incomplete identification information and seperator with no chart in meter box and at wellhead there is 8.625 and 4.5 and 2.375 tubing and valves were closed on the day of my inspection,and after calling company rep stating that production casing has possible hole in it that is why well quit producing.

PLUG WELL OR REPAIR CASING AND PUT BACK INTO PRODUCTION. Failure to comply may result in bond forfieture.

For data sources see[2]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20. 
  2. "Ohio Department of Natural Resources RBDMS". [2]. 2015-06-19. Retrieved 2015-06-20.