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Well ID: 34-155-23832 | Loading map...
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County: Trumbull | |
Municipality: | |
Operator Name: ENERVEST OPERATING L | |
Well Pad ID: | |
Farm/Lease Name: | |
First Permit Date: | |
Last Permit Date: | |
Spud Date: 2007-07-02 | |
Unconventional: No | |
Configuration: Vertical | |
Well Status: Producing | |
Violations: 0 | |
Latitude: 41.42229427 | |
Longitude: -80.52896293 |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
---|---|---|---|---|---|---|
2007-0 | 11592.0 | 0.0 | ||||
2008-0 | 26229.0 | 85.0 | ||||
2009-0 | 9749.0 | 0.0 | ||||
2010-0 | 9187.0 | 50.0 | ||||
2011-0 | 4998.0 | 0.0 | ||||
2012-0 | 3686.0 | 0.0 | ||||
2013-0 | 3193.0 | 38.0 | ||||
2014-0 | 3087.0 | 365.0 | 0.0 | 365.0 |
For data sources see[1]
INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID | VIOLATION CODE | VIOLATION COMMENT |
---|---|---|---|---|---|---|
-1417656892 | 2014-04-22 | My inspection found the well in production. The well was equipped with a plunger lift unit. There was a 4 PVC pipe placed on top of the rabbit section of the well to mark the location. The tank battery consisted of a 100 barrel production tank, a 50 barrel brine tank, and a separator. The dike met containment requirements. An identification sign was properly posted. There was a 7 day production chart inside the separator. The lease road was in stable condition. | ||||
-1793979625 | 2007-07-05 | Union Drilling Co. shut-down for repairs . | ||||
-275863796 | 2010-06-21 | no violations . |
For data sources see[2]