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34-151-21190

Well Details

Well ID: 34-151-21190
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County: Stark
Municipality:
Operator Name: ALLIANCE PETROLEUM CORPORATION
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 1967-05-26
Unconventional: No
Configuration: Vertical
Well Status: Plugged and Abandoned
Violations: 0
Latitude: 40.78992338
Longitude: -81.30788362

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
1982-0 0.0 68.0
1983-0 0.0 205.0
1984-0 0.0 403.0
1985-0 0.0 217.0
1986-0 0.0 149.0
1987-0 0.0 147.0
1988-0 0.0 140.0
1989-0 0.0 149.0
1990-0 0.0 134.0
1991-0 0.0 35.0
1992-0 0.0 120.0
1993-0 0.0 48.0
1994-0 0.0 76.0
1995-0 0.0 80.0
1998-0 0.0 154.0
1999-0 0.0 148.0
2000-0 0.0 36.0

For data sources see[1]

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
1204661064 2008-03-04 Located the plugging location.
1205241301 2008-03-07 Pumped Clinton plug thru tubing. Appalachian Well Services cut the casing at 3355'.
1205262997 2008-03-11 Pluggers circulated the well with gel. The rig pulled 1 joint of 5-1/2 diameter casing. Pluggers pumped the Big Lime plug. The rig pulled 1 joint of casing. The rig attempted to pull another joint, but the casing hung and the rig was unable to pull the casing up and out of the cement. The casing shooters were called and the casing was cut at 928'. Circulation was established. The 8-5/8 casing plug will be pumped on Wednesday.
1587866216 2013-07-03 Flow lines left in ground, and in the woods adjacent to the access road. Referred to inspector Roush.
1718791230 2008-03-06 Plugger's, Inc. is on the location and is pulling rods.
1764942962 2008-03-10 The rig was unable to pull the 5-1/2 dia casing. Pluggers, Inc. circulated on the casing and circulated out oil. The rig tried to pull the casing again. The casing is free, but the rig is unable to pull it up more than a few feet. Appalachian Well Services ran a bond log to determine where the casing was hung. The bond log showed caving or bridging at 1100'. Pluggers, Inc. will circulate gel on Tuesday in an attempt to free the casing.
-560217506 2009-05-20 This well was plugged and abandoned on 3-12-2008. The location is rough graded, there is no vegetation growing, and I have no landowner waiver. I did not pass the Final Restoration at this time.
PL5644 Preliminary Restoration done information from Data Point

For data sources see[2]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20. 
  2. "Ohio Department of Natural Resources RBDMS". [2]. 2015-06-19. Retrieved 2015-06-20.