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34-093-21246

Well Details

Well ID: 34-093-21246
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County: Lorain
Municipality:
Operator Name: ROBERTS BOB / WILDWOOD PARK
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 1984-02-08
Unconventional: No
Configuration: Vertical
Well Status: Producing
Violations: 0
Latitude: 41.33869958
Longitude: -81.90762003

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
1985-0 12050.0 0.0
1986-0 10905.0 0.0
1987-0 3179.0 0.0
1988-0 4901.0 0.0
1989-0 1897.0 0.0
1990-0 1193.0 0.0
1991-0 0.0 946.0
1992-0 640.0 16.0
1993-0 738.0 0.0
1994-0 449.0 0.0
1995-0 370.0 0.0
1996-0 393.0 0.0
1997-0 62.0 0.0
1998-0 0.0 0.0

For data sources see[1]

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
1087479368 2004-06-17 Called by Rhonda Vedda at 11036 East River Rd. that a gas leak in yard. Gas is bubbling at 4% lel. Sales line leading from well crossing SR 252. Called Jim Gessel of Dome Drilling. Jim advised he sold well to Bob Roberts but will repair the gas leak for him. Well is used for domestic house gas only. Compliance Notice
1087479368 2004-06-17 Called by Rhonda Vedda at 11036 East River Rd. that a gas leak in yard. Gas is bubbling at 4% lel. Sales line leading from well crossing SR 252. Called Jim Gessel of Dome Drilling. Jim advised he sold well to Bob Roberts but will repair the gas leak for him. Well is used for domestic house gas only. Compliance Notice
1089219472 2004-07-07 Gas leak has been repaired. Case # 04-010
-485034269 2014-07-18 Inspected production well on 07/18/2014. The well is equipped with a wellhead with a swedge, gauge, and elbow. No well identification is posted. The well did not appear to be hooked up at the time of the inspection. No tanks were noted nearby. Research into the production history of the well showed that no production has been filed since 1998, therefore the well must be plugged.
PL13351 Preliminary Restoration done information from Data Point

For data sources see[2]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20. 
  2. "Ohio Department of Natural Resources RBDMS". [2]. 2015-06-19. Retrieved 2015-06-20.