If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.
powered by ChangeDetection
Well ID: 34-119-27343 | Loading map...
{"type":"SATELLITE","minzoom":false,"maxzoom":false,"types":["ROADMAP","SATELLITE","HYBRID","TERRAIN"],"mappingservice":"googlemaps3","width":"100%","height":"350px","centre":false,"title":"","label":"","icon":"","visitedicon":"","lines":[],"polygons":[],"circles":[],"rectangles":[],"wmsoverlay":false,"copycoords":false,"static":false,"zoom":14,"layers":[],"controls":["pan","zoom","type","scale","streetview","rotate"],"zoomstyle":"DEFAULT","typestyle":"DEFAULT","autoinfowindows":false,"resizable":false,"kmlrezoom":false,"poi":true,"markercluster":false,"clustergridsize":60,"clustermaxzoom":20,"clusterzoomonclick":true,"clusteraveragecenter":true,"clusterminsize":2,"imageoverlays":[],"kml":[],"gkml":[],"searchmarkers":"","enablefullscreen":false,"scrollwheelzoom":false,"locations":[{"text":"","title":"","link":"","lat":40.07540254,"lon":-82.18333436,"icon":""}]} |
County: Muskingum | |
Municipality: | |
Operator Name: DALTON & HANNA LTD | |
Well Pad ID: | |
Farm/Lease Name: | |
First Permit Date: | |
Last Permit Date: | |
Spud Date: 2011-08-24 | |
Unconventional: No | |
Configuration: Vertical | |
Well Status: Dry and Abandoned | |
Violations: 0 | |
Latitude: 40.07540254 | |
Longitude: -82.18333436 |
INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID | VIOLATION CODE | VIOLATION COMMENT |
---|---|---|---|---|---|---|
1317137863 | 2011-09-27 | Rig at 1708', in the Big Cinnnamon. Odor of gas in the samples. Dennis and Dean Moran were onsite. | ||||
1320260180 | 2011-10-24 | Rig set 2975' of casing in 2977' of open 6 1/2 hole. They ran a float shoe on bottom and centralizers on the 2nd, 4th and 6th joint from the bottom. They also ran one 4.5 basket 800' down from surface. Good circulation and Cemenco ran 50 sacks regular Class A cement. Cement should cover the Newburg formation. | ||||
1339696682 | 2012-06-14 | Set bottom plug with clay and rip 4.5 casing @ 2480'. Washed in Lime plug. | ||||
1339773389 | 2012-06-16 | Finished plugging to surface this date. | ||||
1406160451 | 2011-10-04 | Rig is drilling at a depth of 2300' in the Big Lime. | ||||
-1536227641 | 2011-11-18 | This well has been drilled, 4.5 production casing has been set and it has a 4x2 reducer with valve on it. The production casing was set to allow for open hole completion. Prior to fracing, attempts were made to bail the hole dry but water kept encroaching. The frac was postponed and the company is evaluating the well. | ||||
-1947840229 | 2011-10-11 | The rig is drilling in the Big Lime at at depth of 2630'. | ||||
2110893074 | 2011-10-21 | Rig drilling at a depth of 2930' in the Packer Shell. | ||||
-2129550112 | 2011-12-28 | Well is drilled and not completed.Company is still evaluating well.No change. | ||||
266961787 | 2011-12-01 | Well drilled not fraced yet. Pits Closed. | ||||
289146239 | 2011-11-25 | Well has been drilled but not fraced.No change. | ||||
409615518 | 2011-09-12 | Moran set surface pipe and Cemenco cemented casing in place. Circulation was established. | ||||
-967616107 | 2011-09-16 | Rig ran 796' of 7 casing. |
For data sources see[1]