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34-119-27343

Well Details

Well ID: 34-119-27343
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County: Muskingum
Municipality:
Operator Name: DALTON & HANNA LTD
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 2011-08-24
Unconventional: No
Configuration: Vertical
Well Status: Dry and Abandoned
Violations: 0
Latitude: 40.07540254
Longitude: -82.18333436

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
1317137863 2011-09-27 Rig at 1708', in the Big Cinnnamon. Odor of gas in the samples. Dennis and Dean Moran were onsite.
1320260180 2011-10-24 Rig set 2975' of casing in 2977' of open 6 1/2 hole. They ran a float shoe on bottom and centralizers on the 2nd, 4th and 6th joint from the bottom. They also ran one 4.5 basket 800' down from surface. Good circulation and Cemenco ran 50 sacks regular Class A cement. Cement should cover the Newburg formation.
1339696682 2012-06-14 Set bottom plug with clay and rip 4.5 casing @ 2480'. Washed in Lime plug.
1339773389 2012-06-16 Finished plugging to surface this date.
1406160451 2011-10-04 Rig is drilling at a depth of 2300' in the Big Lime.
-1536227641 2011-11-18 This well has been drilled, 4.5 production casing has been set and it has a 4x2 reducer with valve on it. The production casing was set to allow for open hole completion. Prior to fracing, attempts were made to bail the hole dry but water kept encroaching. The frac was postponed and the company is evaluating the well.
-1947840229 2011-10-11 The rig is drilling in the Big Lime at at depth of 2630'.
2110893074 2011-10-21 Rig drilling at a depth of 2930' in the Packer Shell.
-2129550112 2011-12-28 Well is drilled and not completed.Company is still evaluating well.No change.
266961787 2011-12-01 Well drilled not fraced yet. Pits Closed.
289146239 2011-11-25 Well has been drilled but not fraced.No change.
409615518 2011-09-12 Moran set surface pipe and Cemenco cemented casing in place. Circulation was established.
-967616107 2011-09-16 Rig ran 796' of 7 casing.

For data sources see[1]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20.