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Well ID: 34-055-20097 | Loading map...
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County: Geauga | |
Municipality: | |
Operator Name: ENERVEST OPERATING L | |
Well Pad ID: | |
Farm/Lease Name: | |
First Permit Date: | |
Last Permit Date: | |
Spud Date: 1973-10-09 | |
Unconventional: No | |
Configuration: Vertical | |
Well Status: Producing | |
Violations: 0 | |
Latitude: 41.48200992 | |
Longitude: -81.12974673 |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
---|---|---|---|---|---|---|
1985-0 | 3693.0 | 33.0 | ||||
1986-0 | 2019.0 | 0.0 | ||||
1987-0 | 1538.0 | 0.0 | ||||
1991-0 | 2270.0 | 0.0 | ||||
1992-0 | 1754.0 | 57.0 | ||||
1993-0 | 1365.0 | 64.0 | ||||
1994-0 | 2953.0 | 0.0 | ||||
1995-0 | 2865.0 | 0.0 | ||||
1996-0 | 3238.0 | 79.0 | ||||
1997-0 | 2529.0 | 0.0 | ||||
1998-0 | 1943.0 | 76.0 | ||||
1999-0 | 944.0 | 0.0 | ||||
2000-0 | 1534.0 | 0.0 | ||||
2001-0 | 1442.0 | 0.0 | ||||
2002-0 | 1670.0 | 0.0 | ||||
2003-0 | 568.0 | 0.0 | ||||
2004-0 | 524.0 | 0.0 | ||||
2005-0 | 812.0 | 0.0 | ||||
2006-0 | 786.0 | 60.0 | ||||
2007-0 | 872.0 | 0.0 | ||||
2008-0 | 1074.0 | 0.0 | ||||
2010-0 | 821.0 | 0.0 | ||||
2011-0 | 1046.0 | 33.0 | ||||
2012-0 | 794.0 | 0.0 | ||||
2013-0 | 595.0 | 0.0 | ||||
2014-0 | 529.0 | 365.0 | 0.0 | 365.0 |
For data sources see[1]
INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID | VIOLATION CODE | VIOLATION COMMENT |
---|---|---|---|---|---|---|
1398449343 | 2014-04-25 | My inspection found the well to be equipped with a plunger lift unit. The tank battery consists of a 210 BBL production tank, a 100 BBL production tank, a 50 BBL poly brine tank, and a mechanical separator. The 210 BBL tank is leaking around the base and the dike needs rebuilt. The fence surrounding the tank battery needs repaired. The proper identification is located on the tank battery. The lease road is in stable condition. I have contacted the company about having the issues corrected. | ||||
-1820891741 | 2014-12-18 | My inspection found the 210 BBL tank that was leaking has been removed from the tank battery. The dike around the tank battery has been rebuilt. The fence surrounding the tank battery has been repaired. No other changes to the location since my last inspection. No violations found. |
For data sources see[2]