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Well ID: 34-155-24016 | Loading map...
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County: Trumbull | |
Municipality: | |
Operator Name: STRYKER ENERGY LLC | |
Well Pad ID: | |
Farm/Lease Name: | |
First Permit Date: | |
Last Permit Date: | |
Spud Date: 2010-02-01 | |
Unconventional: No | |
Configuration: Vertical | |
Well Status: Producing | |
Violations: 0 | |
Latitude: 41.46918972 | |
Longitude: -80.59939006 |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
---|---|---|---|---|---|---|
2010-0 | 3212.0 | 109.0 | ||||
2011-0 | 503.0 | 49.0 | ||||
2012-0 | 0.0 | 0.0 | ||||
2013-0 | 0.0 | 0.0 | ||||
2014-0 | 0.0 | 0.0 | 0.0 | 0.0 |
For data sources see[1]
INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID | VIOLATION CODE | VIOLATION COMMENT |
---|---|---|---|---|---|---|
-1015311625 | 2010-03-03 | Drilling pits have been closed , | ||||
1363873667 | My inspection found the well not in production. The well was equipped with a plunger lift unit. There was black 1 poly tubing wrapped around the well. The tank battery contained one, 100 barrel production tank, one, 50 barrel brine tank, and a separator. It was surrounded by a dike capable of meeting containment requirements. The identification sign on the production tank was faded and unreadable. There was a 7 day production chart in the separator dated 4/2/2012. I researched our database and found the last reported production was in 2010. | |||||
1701513542 | 2010-02-02 | Kilbarger drilling at 154' . No violations . | ||||
-2017604751 | 2010-02-04 | Kilbarger drilling company . No violations . | ||||
-2120826228 | 2010-02-01 | Kilbager rigging up . No violations . | ||||
30286736 | 2013-04-03 | My inspection found the proper identification posted on the production tank per my request. | ||||
372945829 | 2013-03-21 | My inspection found this well not in production. The well was equipped with a plunger lift unit. There was 1 black tubing wrapped around the well. The tank battery contained one, 100 barrel production tank, one, 50 barrel brine tank, and a separator. It was surrounded by a dike capable of meeting containment requirements. The separator had a 7 day production chart that was dated 4/2/2012. The identification was faded and hard to read. There was a plug on the load line. The last reported production was in 2010. I called Stryker Energy at 440-446-9198. I was informed the company sold the sales line to Dominion in 2011. Stryker was in the process of working with Dominion on getting this well back into production. I instructed Stryker to replace the identification sign and remove the tubing from around the well. Also, I told them I would re-inspection the well by 5/1/2013 to see if it was placed back into production. | ||||
-932951842 | 2010-02-08 | Drilling pits showed no violations . |
For data sources see[2]