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34-153-22193

Well Details

Well ID: 34-153-22193
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County: Summit
Municipality:
Operator Name: BERRY ENTERPRISES INC
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 1987-01-23
Unconventional: No
Configuration: Vertical
Well Status: Producing
Violations: 0
Latitude: 40.96965779
Longitude: -81.62958418

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
1987-0 3690.0 76.0
1989-0 301.0 95.0
1990-0 13082.0 0.0
1991-0 1531.0 0.0
1994-0 0.0 0.0
2008-0 0.0 0.0
2009-0 53.0 0.0
2010-0 66.0 0.0
2011-0 32.0 0.0
2012-0 33.0 0.0
2013-0 2.0 0.0
2014-0 331.0 360.0 0.0 360.0

For data sources see[1]

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
1220731038 2014-03-18 FOLLOW UP TO NOV # 2084977928 Compliance follow up inspection of this Plunger lift ( rabbit ) well. I inspected this well on 3/18/2014. The construction of the well is 4.5 casing with 2 tubing inside. The Demco gate valve is closed thus shutting in the well. Further, the well is not capable of production as the tubing is disconnected from the flowline. The required identification signage was absent from the wellhead. The tank battery has been removed. A orange 1 house gasline is present , but not connected to anything. The Owner of the well has reported non-commerical levels of production for the years 2008 to 2012. The rathole and mousehole need plugging.
1426076348 2014-11-24 I re-inspected the Kiminecz # 2 on 11/24/2014. The tank battery issues ( locks, leaks and dikes ) had been addressed and been corrected. The flow line had been fixed and tied to the well. The rat and mouse holes had been filled. I spoke with Mr. Berry on location who was trying to get the well to unload and back into production. I will confirm production when 2014 production numbers are reported.
-2080200394 2005-02-24 FOLLOW UP TO NOV # 2084977928 Status check inspection of this rabbit well. The last reported production from this well was in 1991. The well must either be plugged and abandoned or placed back into production.
2084977928 2005-02-24 Status check inspection of this rabbit well. The last reported production from this well was in 1991. The well must either be plugged and abandoned or placed back into production.

For data sources see[2]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20. 
  2. "Ohio Department of Natural Resources RBDMS". [2]. 2015-06-19. Retrieved 2015-06-20.