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34-167-29618

Well Details

Well ID: 34-167-29618
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County: Washington
Municipality:
Operator Name: GREEN HUNTER WATER LLC
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 2007-01-02
Unconventional: No
Configuration: Vertical
Well Status: Active Injection
Violations: 0
Latitude: 39.392185
Longitude: -81.23614409

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
2007-0 8200.0 0.0
2008-0 5538.0 0.0
2009-0 3159.0 0.0
2010-0 2574.0 0.0
2011-0 4939.0 0.0

For data sources see[1]

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
-1014264494 2014-08-14 Well is still down for repair it appears that packer or tubing has lost integrity.
-1024802833 2014-03-20 Inspection revealed that injection pump was in operation today.

Note: Called company rep to discuss making final plan to make permanent upgrades to facility.

-103274041 2014-05-05 Inspection revealed that well is still down waiting on plan to correct equalization issues.
 Note: Company has contacted Central Office and they are working on proposal to repair well.
-1120138162 2014-01-28 Inspection revealed that injection pump was not in operation during my inspection and it was noted that one Oil Hauler's tanker was unloading at site during my inspection.
1185456986 2007-07-25 Inspection this day found well producing with rabbit, tank freshly painted, will have ID's up soon, good dike, current chart in meter. Location has been reclaimed, landowner farming ground.
1343814043 2013-12-13 Inspection revealed that injection pump was in operation today and it was noted that annulus pressure has fallen off and I told operator to arrange to have positive pressure applied to annulus ASAP.
1352945780 2013-09-13 On site to pressure test recently installed flow line they pressured up to 1750 psi and we monitored pressure and visually inspected line to check for possible leakage none were noted at this time.
1355530400 2012-12-14 On site to witness Packer and tubing run into well to prepare well for conversion to UIC facility, Key Energy ran packer and 4033' of tubing today will finish running tubing and test integrity on 12/17/2012.

Note: Two Central Office personnel on site to witness job also.

1356100662 2012-12-17 On site to witness setting of packer and witness pressure testing of annulus.

Note: Packer set at 7238.1 and new 2.375 Baker A-3 set lock set under 10K compression perforations@7324'-7332' (32) shots Pumped 500 gal of 15% acid and Baker pumped at a rate of 1.2 bpm at 1540 psi will further test tomorrow with salt brine.

137114550 2013-11-20 Inspection revealed that injection pump was in operation today and I reminded operator to submit plans for permanent facility construction plan.
1379022400 2013-09-12 Inspection revealed that owner is in process of constructing temporary injection site facility they have 2-500 bbl tanks within dike area and are currently placing injection pump at site and also they have constructed a small building to be used as a electrical building, they plan on having facility up and running by next week.

Note: Informed owner that a barrel counter will need to be in place before well goes into operation.

149172631 2012-12-27 No activity at site today due to weather conditions.
1547888243 2014-01-06 Inspection revealed that injection pump was in operation today and it was noted that operator called and stated that they had a tanker truck off of the lease road and that have called for two additional vacuum trucks to offload stuck truck too ensure that no brine water could possibly enter back waters of the waterway.
-1592099323 2009-04-30 Inspection this day found well producing with rabbit, tank has good ID's, good dike, current chart in meter.
1602814986 2013-10-01 On site to witness company owned service rig pull tension on tubing to enable them to tighten up tubing head they were able to fix tubing head and once they repacked head they applied positive pressure to annulus and we monitored pressure for 15 minutes with no decline in pressure.
1907313891 2014-02-12 Inspection revealed that injection pump was in operation during my inspection and it was noted that one Oil Haulers tanker was unloading at site during my inspection.
-1946385466 2012-12-11 Key Energy moving service rig on site to prepare well for injection test they will remove current tubing and sand pump well if needed and then place packer and new tubing in well before performing test on said well.
2109637821 2015-04-10 On site to perform site review for possible plug back operation in the near future once permit is issued.
297421703 2014-04-10 Inspection revealed that well was shut in on the day of my inspection and I called owner too get update on why the well is shut in at this time and he stated that they were doing a flow back test in preparation for tubing replacement.
343282651 2013-12-02 Inspection revealed that injection pump was not in operation today due to maximum pressure.
-344814732 2012-12-12 Service rig on site preparing to pull tubing from well and then run bare tools in well to confirm total depth and then run new tubing and packer into well to do injection test in the Medina Sand.
-371556428 2014-07-30 Inspection revealed that well has equalized and owner is waiting on service rig to pull packer and tubing from well and possibly recomplete well in a more productive injection zone.
-413279439 2013-10-03 On site to witness 1000 gal acid job preformed on said well Producers Services pumped 500 gall into formation and we let it soak for 15 min and then they pumped additional 500 gal and let it soak for 30 min and then they performed pressure testing on formation.
-445858971 2012-12-13 Stopped by service rig for update they were pulling 2.375 tubing today and if all goes well start packer and tubing in well tomorrow.
-536852463 2014-06-16 Inspection revealed that well is down waiting on company to submit work over plan to repair/replace packer or tubing string.
76277932 2010-12-28 Inspection this day found well producing with rabbit - this well had big show in Cow Run when drilled, never went back to produce it yet. Tank has good ID's, current chart in meter.
84301181 2013-11-06 Inspection revealed that injection pump was in operation and I told operator to ask for extension on temporary injection facility and submit plan for facility construction.
-950254579 2015-06-08 Well is not in operation at this time owner is waiting on plug back permit to be issued.

For data sources see[2]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20. 
  2. "Ohio Department of Natural Resources RBDMS". [2]. 2015-06-19. Retrieved 2015-06-20.