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Well ID: 34-059-21748 | Loading map...
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County: Guernsey | |
Municipality: | |
Operator Name: SOUND ENERGY CO INC | |
Well Pad ID: | |
Farm/Lease Name: | |
First Permit Date: | |
Last Permit Date: | |
Spud Date: 1974-10-19 | |
Unconventional: No | |
Configuration: Vertical | |
Well Status: Producing | |
Violations: 0 | |
Latitude: 40.1306833 | |
Longitude: -81.33604847 |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
---|---|---|---|---|---|---|
1984-0 | 0.0 | 0.0 | ||||
1985-0 | 0.0 | 0.0 | ||||
1989-0 | 0.0 | 0.0 | ||||
1990-0 | 0.0 | 0.0 | ||||
1991-0 | 0.0 | 0.0 | ||||
1992-0 | 0.0 | 0.0 | ||||
1993-0 | 0.0 | 0.0 | ||||
1994-0 | 0.0 | 0.0 | ||||
1995-0 | 0.0 | 0.0 | ||||
1996-0 | 0.0 | 0.0 | ||||
1997-0 | 0.0 | 0.0 | ||||
1998-0 | 0.0 | 0.0 | ||||
1999-0 | 0.0 | 0.0 | ||||
2000-0 | 0.0 | 0.0 | ||||
2001-0 | 0.0 | 0.0 | ||||
2003-0 | 0.0 | 0.0 | ||||
2004-0 | 0.0 | 0.0 | ||||
2005-0 | 0.0 | 0.0 | ||||
2006-0 | 0.0 | 0.0 | ||||
2007-0 | 0.0 | 0.0 | ||||
2008-0 | 0.0 | 0.0 | ||||
2009-0 | 0.0 | 0.0 | ||||
2010-0 | 0.0 | 0.0 | ||||
2011-0 | 0.0 | 0.0 | ||||
2012-0 | 0.0 | 0.0 | ||||
2013-0 | 0.0 | 0.0 | ||||
2014-0 | 0.0 | 0.0 | 0.0 | 0.0 |
For data sources see[1]
INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID | VIOLATION CODE | VIOLATION COMMENT |
---|---|---|---|---|---|---|
-111880666 | 2006-09-01 | PRODUCING WELL. | Compliance Notice | |||
1131552943 | 2005-11-09 | STATUS CHECK | ||||
1289i26153843 | 2001-05-31 | STATUS CHECK | ||||
1337882248 | 2013-10-24 | On the day of my inspection, I found no change in the status of the well since my last inspection done on 05/26/2013, I placed a phone call to Bruce Levengood with Sound Energy for an up date on a service rig availability to plug. | ||||
1361899803 | 2013-02-25 | On the day of my inspection I reviewed the Divisions production records and found there had been no production recorded from the year of 1984 to 2013, after speaking with Sound Energy I was told the well had never been produced. My inspection at the well site reveled eight inch casing with four inch production casing that had been broken off, there is (1) one hundred barrel production tank sitting on the well location. The requirements to meet the Divisions standards will be, to make the well capable of commercial production within sixty days, or plugging is required within sixty days, legibly identify well. | ||||
1367261754 | 2013-04-29 | No change in the status of the well, Sound Energy requested a sixty day extension for plugging and they are currently working with the landowner to resolve the lease issue. | ||||
1379520580 | 2013-09-17 | Pryor to my inspection, I made a phone call to Sound Energy and spoke with Bruce Levengood about the status and condition of the this well, Mr. Levengood asked me for a sixty day allowance to get a service rig on site and run a bond log to find out if the integrity of the 4.5 casing is any good before plugging, I agreed to the sixty day allowance, I also asked Mr. Levengood if he would take care of the one hundred barrel tank that is on site as well as fencing of the well head. The status of the well has not change since my last inspection. | ||||
1383148410 | 2013-10-30 | On the day of my inspection, I witnessed the rig crew for Knox Energy and Bruce Levengood with Sound Energy packing off the well and putting a 4x2 swedge with a gate valve in the well. The well was drilled in 1973 but was never perforated or produced, Sound Energy is going to pressure test the casing and at that point decide if they will produce or plug the well. | ||||
1676356591 | 2006-01-10 | WELL PRODUCING | ||||
560908775 | 2015-01-26 | On the day of my inspection following up NOV-1361899803, I witnessed the well was equipped with 8.625 inch casing, 4.5 inch casing with a 4.5 inch to 2 inch swedge with the valve in the closed position. Production equipment included a 100bbl tank in an earthen dike with identification present on the tank. I made a call to Bruce Levengood of Sound Energy requesting an update on the well. He stated that the well had never been completed and a bond log and casing test had been performed. Sound Energy plans on fracing well this summer. |
For data sources see[2]