X

Track changes made to this page

If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.



Privacy policy
Close this window

powered by ChangeDetection

34-155-22679

Well Details

Well ID: 34-155-22679
Loading map...
County: Trumbull
Municipality:
Operator Name: ENERVEST OPERATING L
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 1985-02-08
Unconventional: No
Configuration: Vertical
Well Status: Producing
Violations: 0
Latitude: 41.38520142
Longitude: -80.58429799

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
1985-0 6554.0 69.0
1986-0 16548.0 68.0
1987-0 15080.0 69.0
1988-0 10479.0 69.0
1989-0 6679.0 0.0
1990-0 9807.0 71.0
1991-0 6824.0 0.0
1992-0 3111.0 0.0
1993-0 1595.0 74.0
1994-0 4571.0 36.0
1995-0 3484.0 0.0
1996-0 4678.0 0.0
1997-0 4560.0 59.0
1998-0 3557.0 0.0
1999-0 3312.0 0.0
2000-0 3711.0 0.0
2001-0 2090.0 0.0
2002-0 1049.0 0.0
2003-0 281.0 0.0
2004-0 0.0 0.0
2005-0 0.0 27.0
2006-0 0.0 0.0
2007-0 0.0 0.0
2008-0 3705.0 0.0
2009-0 3230.0 35.0
2010-0 0.0 0.0
2011-0 2380.0 0.0
2012-0 2511.0 28.0
2013-0 2798.0 0.0
2014-0 2417.0 365.0 0.0 365.0

For data sources see[1]

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
-1281511012 2012-08-29 On 8/29/2012, I completed an urban production well inspection status check. My inspection found the well equipped with a plunger lift unit (rabbit) that was in good condition. The tank battery contained one 100 barrel oil/brine storage tank, a separator, and the proper identification posted. I noticed no visible spills or leaks. The lease road was in good condition. There are no violations at this time.
-1401430659 2003-11-20 No annular disposal .
1421326503 2015-01-14 I was on location for a status check. During my inspection, I found the well in production. The well was equipped with a plunger lift assembly. A domestic gas line came off of the 4.5 casing with the flow line ball valve in the open position. The tank battery consisted of a 100 barrel production tank and a mechanical separator. A dike surrounded the tank battery. An identification sign was properly posted on the tank. There was a lock and plug on the load line. A production meter and 16 day chart was installed inside of the separator. The lease road was in stable condition.
1585870703 2009-05-05 no annular disposal .
2042033169 2006-03-24 no violations .
802242190 2010-03-03 no annular disposal .
PL3648 Preliminary Restoration done information from Data Point

For data sources see[2]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20. 
  2. "Ohio Department of Natural Resources RBDMS". [2]. 2015-06-19. Retrieved 2015-06-20.