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34-127-24899

Well Details

Well ID: 34-127-24899
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County: Perry
Municipality:
Operator Name: KILBARGER INVESTMENTS INC
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 1980-11-19
Unconventional: No
Configuration: Vertical
Well Status: Producing
Violations: 0
Latitude: 39.6085523
Longitude: -82.34916543

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
1985-0 268.0 280.0
1986-0 280.0 270.0
1987-0 324.0 181.0
1988-0 457.0 192.0
1989-0 501.0 117.0
1990-0 355.0 144.0
1991-0 317.0 197.0
1992-0 186.0 160.0
1993-0 211.0 39.0
1994-0 108.0 59.0
1995-0 242.0 131.0
1996-0 247.0 116.0
1997-0 289.0 110.0
1998-0
2000-0 270.0 45.0
2001-0 69.0 0.0
2002-0 0.0 0.0
2003-0 0.0 0.0
2004-0 0.0 23.0
2005-0 0.0 0.0
2006-0 0.0 0.0
2007-0 0.0 0.0
2008-0 0.0 0.0
2009-0 0.0 0.0
2010-0 0.0 0.0
2011-0 0.0 0.0
2012-0 0.0 0.0
2013-0 0.0 0.0
2014-0 0.0 365.0 0.0 365.0

For data sources see[1]

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
1102365059 2004-12-06 No I.D. / Using A.D. Compliance Notice
1102365059 2004-12-06 No I.D. / Using A.D. Field Visit or Inspection
1103745120 2004-12-22 A.D. Inspection ( not using A.D. )
1421906160 2010-03-02 An inspection of this well was requested by Central Office to verify Annular Disposal (AD) connection. During the inspection, it was noted that the AD remains disconnected. Note: snow cover at time of inspection.
430956769 2004-12-22 A.D. has been disconnected and I.D on tank. ( RESOLVED )
-663661292 2013-03-14 This well is capable of production. It has a pumping unit on it with rods and 2 tubing. The valves are open. It looks like the land owners are getting house gas off of the well. There is no motor on the unit. I talk with Dan Wrestler from Kilbarger and he is going to bring it up in the morning meeting to get it back in production. He is going to contact me on the 15th of March on the issue.
929096302 2013-07-09 This well is now in-compliance.
PL7168 Preliminary Restoration done information from Data Point

For data sources see[2]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20. 
  2. "Ohio Department of Natural Resources RBDMS". [2]. 2015-06-19. Retrieved 2015-06-20.