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Well ID: 34-119-28547 | Loading map...
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County: Muskingum | |
Municipality: | |
Operator Name: POLING R C CO INC | |
Well Pad ID: | |
Farm/Lease Name: | |
First Permit Date: | |
Last Permit Date: | |
Spud Date: 2005-11-29 | |
Unconventional: No | |
Configuration: Vertical | |
Well Status: Producing | |
Violations: 0 | |
Latitude: 39.84501215 | |
Longitude: -82.03131876 |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
---|---|---|---|---|---|---|
2007-0 | 1984.0 | 0.0 | ||||
2008-0 | 1826.0 | 0.0 | ||||
2009-0 | 2098.0 | 0.0 | ||||
2010-0 | 1830.0 | 0.0 | ||||
2011-0 | 2126.0 | 0.0 | ||||
2012-0 | 3343.0 | 0.0 | ||||
2013-0 | 3090.0 | 0.0 | ||||
2014-0 | 4428.0 | 365.0 | 0.0 | 365.0 |
For data sources see[1]
INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID | VIOLATION CODE | VIOLATION COMMENT |
---|---|---|---|---|---|---|
1143546368 | 2006-03-27 | Location roughed in. Not completed yet. | Compliance Notice | |||
1409831785 | 2014-09-03 | Inspected well based on complaint #4788. The complainant was Abbey Kindler. She noticed the dike around the 100 barrel tank was full of crude oil and had ran over the dike on 8-15-14 around noon. She called on 9-2-14. I revealed that there was a dike that had approximately measured 30'x40'in circumference. There was 1-100 barrel tank and a vertical separator with in the dike. The dike was full of crude oil and had ran over leaving approximately a 20'x30'oil soaked spot. The source of the release inside the dike is unknown at this time. After calling and talking to Dick Poling he would have men and equipment out on site on 9-4-14. The well is equipped with a pumping unit and the production manifold has been shut in.There is prime mover of a natural gas powered single piston motor. The identification is incomplete at the well and the tank. There is second 100 barrel tank down by the entrance with a dike and no identification. The company was instructed to remove all oil and contaminated soil and dispose of properly. The date of cleanup is 9-4-14. Attach all identification to the tanks. Failure to comply will result in further enforcement action. | ||||
1409935715 | 2014-09-04 | Dick Poling called and stated that there was approximately 40 barrel cleaned up. 4 barrel was crude oil the rest was production water. The site was cleaned up and rediked. There was a nipple leaking on the tank. | ||||
1410351937 | 2014-09-09 | Dick Poling called and stated that the well identification has been attached to the tank. I will check at later date. | ||||
1421264992 | 2014-09-22 | I stopped by location and all material has been cleaned up and removed. All identification has been placed at the 1-100 barrel tank battery. There is a new dike constructed around the tank that exceeds the 110% containment. The Compliance Notice # 1409831785 has been resolved on 9-22-14 by Patrick Shreve. | ||||
-1493253582 | 2007-11-07 | Producing, no problems noted. | ||||
416539436 | 2014-09-08 | The contaminated soil has been removed. There was 40 barrel of total fluids removed from area. The only compliance issue was identification not placed on well or tank. | ||||
-505928240 | 2006-12-20 | Producing | ||||
-95741232 | 2006-08-08 | Final grade seeded and mulched |
For data sources see[2]