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34-067-20904

Well Details

Well ID: 34-067-20904
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County: Harrison
Municipality:
Operator Name: ATLAS NOBLE LLC
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 1990-02-07
Unconventional: No
Configuration: Vertical
Well Status: Producing
Violations: 0
Latitude: 40.22411401
Longitude: -81.29269854

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
1990-0 2661.0 0.0
1991-0 3730.0 0.0
1993-0 1946.0 0.0
1994-0 1367.0 0.0
1995-0 1587.0 0.0
1996-0 1372.0 400.0
1997-0 1139.0 0.0
1998-0 1387.0 0.0
1999-0 1875.0 0.0
2000-0 1427.0 0.0
2001-0 1369.0 0.0
2002-0 1605.0 60.0
2003-0 1074.0 0.0
2004-0 1300.0 0.0
2005-0 1289.0 0.0
2006-0 619.0 0.0
2007-0 712.0 0.0
2008-0 1228.0 0.0
2009-0 1014.0 118.0
2010-0 518.0 0.0
2011-0 583.0 0.0
2012-0 0.0 0.0
2013-0 0.0 0.0
2014-0 0.0 0.0 0.0 0.0

For data sources see[1]

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
1375102148 2013-07-25 Arrived on location and found well not in production.Checked production reports and company reported 583 mcf for year 2011 and no production for 2012. Called company and was told that well has been shut-in since aug/ 11/ 2009 because fo a bad flow line. Make well capable of commerical production within 30 days; or plugging is required within 60 days. Failure to comply may result in forfeiture of bond.
1382 PASSED Y WITNESSED 6/10/91 INSPECTOR BRETT FARNSWORTH DATE 06/1019/91 DATA FROM OLD VAX INFO
1770985166 2013-07-25 FOLLOW UP TO NOV # 1375102148 Arrived on location and found well not in production. Checked production reports and company reported 583 mcf for year 2011 and no production for 2012. Called company and was told that well has been shut-in since Aug./ 11/ 2009 because of a bad flow line. Make well capable of commercial production within 30 days; or plugging is required within 60 days. Failure to comply may result in forfeiture of bond.

For data sources see[2]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20. 
  2. "Ohio Department of Natural Resources RBDMS". [2]. 2015-06-19. Retrieved 2015-06-20.