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34-155-20350

Well Details

Well ID: 34-155-20350
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County: Trumbull
Municipality:
Operator Name: DUSTIN ENERGY INC
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 1976-06-30
Unconventional: No
Configuration: Vertical
Well Status: Producing
Violations: 0
Latitude: 41.3129383
Longitude: -80.78119918

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
1984-0 8026.0 0.0
1985-0 7982.0 72.0
1992-0 15597.0 88.0
1993-0 14614.0 93.0
1994-0 14419.0 100.0
1996-0 12741.0 109.0
1997-0 13296.0 92.0
1998-0 10838.0 160.0
1999-0 6233.0 50.0
2000-0 7863.0 62.0
2001-0 6648.0 36.0
2002-0 0.0 35.0
2009-0 0.0 0.0
2010-0 0.0 0.0
2011-0 0.0 0.0
2012-0 0.0 0.0
2013-0 0.0 0.0
2014-0 0.0 0.0 0.0 0.0

For data sources see[1]

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
-1253197594 2008-02-28 Checked well per request from John Flecther [ landowner ] . Inspection showed well is not in production . Records show there has been no production since 2002 . Well is idle . Conf. With John Flemming w/ Great Lakes , he advised me they are going to plug well .
1539774940 2009-01-12 Company sold well to Dustin Energy to put back into production . Violation corrected at this time .
-1925504771 2013-02-12 I was on location for a status check. During my inspection, I found the well equipped as a swab unit. The tank battery consisted of a 100 barrel production tank and a separator. The proper identification was posted. It was surrounded by a locked chain link fence. A weathered dike surrounded the production tank. It was surrounded by a locked chain link fence. The lease road was in stable condition and shared with an Enervest Operating well: 2-3532. Our database shows zero production reported for over 2 years. I called Bill Templeton at 330-240-5573. I informed him a compliance notice would be issued to plug or produce by 6/1/2013.
-869516230 2013-11-04 I called Bill Templeton concerning plugging or producing the well. Bill requested an extension to the beginning of summer for 2014. During the extension, Bill stated he is working on getting a swab rig to see if the well can be placed into production.

For data sources see[2]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20. 
  2. "Ohio Department of Natural Resources RBDMS". [2]. 2015-06-19. Retrieved 2015-06-20.