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Well ID: 34-155-22956 | Loading map...
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County: Trumbull | |
Municipality: | |
Operator Name: ENERVEST OPERATING L | |
Well Pad ID: | |
Farm/Lease Name: | |
First Permit Date: | |
Last Permit Date: | |
Spud Date: 1986-06-27 | |
Unconventional: No | |
Configuration: Vertical | |
Well Status: Producing | |
Violations: 0 | |
Latitude: 41.1430009 | |
Longitude: -80.77146503 |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
---|---|---|---|---|---|---|
1987-0 | 0.0 | 161.0 | ||||
1988-0 | 20835.0 | 186.0 | ||||
1989-0 | 18600.0 | 86.0 | ||||
1990-0 | 11978.0 | 0.0 | ||||
1991-0 | 11607.0 | 0.0 | ||||
1992-0 | 10425.0 | 52.0 | ||||
1993-0 | 9637.0 | 39.0 | ||||
1994-0 | 8890.0 | 0.0 | ||||
1995-0 | 9109.0 | 41.0 | ||||
1996-0 | 8422.0 | 39.0 | ||||
1997-0 | 5471.0 | 0.0 | ||||
1998-0 | 5089.0 | 27.0 | ||||
1999-0 | 1251.0 | 0.0 | ||||
2000-0 | 2675.0 | 0.0 | ||||
2001-0 | 3748.0 | 25.0 | ||||
2002-0 | 4330.0 | 0.0 | ||||
2003-0 | 3456.0 | 0.0 | ||||
2004-0 | 5297.0 | 0.0 | ||||
2005-0 | 4147.0 | 0.0 | ||||
2006-0 | 5200.0 | 29.0 | ||||
2007-0 | 4629.0 | 0.0 | ||||
2008-0 | 3914.0 | 0.0 | ||||
2009-0 | 3531.0 | 0.0 | ||||
2010-0 | 0.0 | 32.0 | ||||
2011-0 | 3617.0 | 0.0 | ||||
2012-0 | 3493.0 | 0.0 | ||||
2013-0 | 3315.0 | 0.0 | ||||
2014-0 | 2921.0 | 365.0 | 0.0 | 365.0 |
For data sources see[1]
INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID | VIOLATION CODE | VIOLATION COMMENT |
---|---|---|---|---|---|---|
-2004804953 | 2014-04-16 | My inspection found the well in production. The well was equipped with a plunger lift unit. The tank battery consisted of a 100 barrel production tank and a separator. The dike was weathered and not capable of meeting containment requirements. A bull plug was installed on the load line. There was a 16 day production chart inside the separator. An identification sign was properly posted. The lease road was in stable condition. The well was placed into production prior to House Bill 278. I called Larry, the field supervisor. I instructed Larry to build a new dike. | ||||
PL3448 | Preliminary Restoration done information from Data Point |
For data sources see[2]