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34-155-23372

Well Details

Well ID: 34-155-23372
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County: Trumbull
Municipality:
Operator Name: ENERVEST OPERATING L
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 1990-10-24
Unconventional: No
Configuration: Vertical
Well Status: Producing
Violations: 0
Latitude: 41.16412673
Longitude: -80.75238384

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
1991-0 19269.0 301.0
1992-0 15175.0 113.0
1993-0 12197.0 47.0
1994-0 8181.0 0.0
1995-0 8031.0 48.0
1996-0 7774.0 50.0
1997-0 5596.0 0.0
1998-0 4391.0 0.0
1999-0 1513.0 0.0
2000-0 2230.0 51.0
2001-0 3296.0 0.0
2002-0 4414.0 0.0
2003-0 3004.0 0.0
2004-0 5052.0 0.0
2005-0 4412.0 0.0
2006-0 5460.0 58.0
2008-0 3990.0 0.0
2009-0 3887.0 0.0
2010-0 0.0 0.0
2011-0 3106.0 41.0
2012-0 2971.0 0.0
2013-0 2537.0 0.0
2014-0 2276.0 365.0 0.0 365.0

For data sources see[1]

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
2075542035 2004-03-10 Restoration approved .
-436310902 2014-04-16 My inspection found the well in production. The well was equipped with a plunger lift unit. The tank battery consisted of a 100 barrel production tank and a separator. The dike met containment requirements. Identification signs were posted at the production tank. A bull plug was installed on the load line. Chain link fences surrounded the production equipment and well. The lease road was in stable condition with locked gate at the entrance. The well was placed into production prior to House Bill 278.

For data sources see[2]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20. 
  2. "Ohio Department of Natural Resources RBDMS". [2]. 2015-06-19. Retrieved 2015-06-20.