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Well ID: 34-073-62336 |
County: Hocking |
Municipality: |
Operator Name: KILBARGER INVESTMENTS INC |
Well Pad ID: |
Farm/Lease Name: |
First Permit Date: |
Last Permit Date: |
Spud Date: 1923-08-16 |
Unconventional: No |
Configuration: Vertical |
Well Status: Plugged and Abandoned |
Violations: 0 |
Latitude: |
Longitude: |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
---|---|---|---|---|---|---|
1987-0 | 0.0 | 73.0 | ||||
1988-0 | 0.0 | 74.0 | ||||
1995-0 | 0.0 | 0.0 | ||||
1996-0 | 0.0 | 0.0 | ||||
1998-0 | 0.0 | 0.0 | ||||
1999-0 | 0.0 | 0.0 | ||||
2000-0 | 0.0 | 0.0 | ||||
2001-0 | 0.0 | 0.0 | ||||
2002-0 | 0.0 | 0.0 | ||||
2003-0 | 0.0 | 0.0 | ||||
2004-0 | 0.0 | 0.0 | ||||
2005-0 | 0.0 | 0.0 | ||||
2006-0 | 0.0 | 316.0 | ||||
2007-0 | 0.0 | 320.0 | ||||
2008-0 | 157.0 | |||||
2009-0 | 0.0 | 226.0 | ||||
2010-0 | 0.0 | 154.0 | ||||
2011-0 | 0.0 | 232.0 | ||||
2012-0 | 0.0 | 0.0 | ||||
2013-0 | 0.0 | 11.0 |
For data sources see[1]
INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID | VIOLATION CODE | VIOLATION COMMENT |
---|---|---|---|---|---|---|
-1019144220 | 2012-12-27 | Spoke with Monica Scmelzer about this well and one other well on the lease. She stated that their attorneys had submitted an offer to the property owner's attorneys earlier this year and no reply has been made. | Compliance Notice | |||
-1019144220 | 2012-12-27 | Spoke with Monica Scmelzer about this well and one other well on the lease. She stated that their attorneys had submitted an offer to the property owner's attorneys earlier this year and no reply has been made. | Compliance Notice | |||
-1019144220 | 2012-12-27 | Spoke with Monica Scmelzer about this well and one other well on the lease. She stated that their attorneys had submitted an offer to the property owner's attorneys earlier this year and no reply has been made. | Compliance Notice | |||
-1019144220 | 2012-12-27 | Spoke with Monica Scmelzer about this well and one other well on the lease. She stated that their attorneys had submitted an offer to the property owner's attorneys earlier this year and no reply has been made. | Compliance Notice | |||
-1019144220 | 2012-12-27 | Spoke with Monica Scmelzer about this well and one other well on the lease. She stated that their attorneys had submitted an offer to the property owner's attorneys earlier this year and no reply has been made. | Compliance Notice | |||
-1019144220 | 2012-12-27 | Spoke with Monica Scmelzer about this well and one other well on the lease. She stated that their attorneys had submitted an offer to the property owner's attorneys earlier this year and no reply has been made. | Compliance Notice | |||
1037785802 | 2014-09-10 | Rods and tubing have been pulled. Production casing is 3, Kilbarger set to place bottom plug on 09/11/14. | ||||
1075907254 | 2014-09-18 | Kilbarger placing prepared clay in the well bore. This is the top plug and will be left open for 1 week to allow for settlement. | ||||
1319737146 | 2011-10-26 | An inspection conducted with Dan Goins, Inspector 3 for the South region Division of Oil and Gas, presented three issues. There was oily material around well, well head did not have a dike, and gas was being vented from the well head. All oily material needs to be cleaned up around well site. Well head needs to have a dike contracted. A flare needs to be built compliant to 1501:9-9-05 (B). | ||||
1320842558 | 2011-11-08 | After a field inspection conducted on 10/26/11, an agent of the landowner's estate, Chris Eiben, notified Dan Goins Inspector 3 for the South region Division of Oil and Gas, and I of a telephone conversation between he and Jeanie Schmelzer via e-mail. He alleges that Jeanie has no records of oil sold from the lease. 154 barrels of oil was the reported production for this well in the year 2010. | ||||
1375864145 | 2008-04-21 | A follow-up inspection revealed compliance. | ||||
1492142365 | 2014-09-11 | Formation Cementing set bottom plug. The 2 7/8 tubing will be shot off at a later date. | ||||
-1537475763 | 2011-11-08 | FOLLOW UP TO NOV # 1320842558 After a field inspection conducted on 10/26/11, an agent of the landowner's estate, Chris Eiben, notified Dan Goins Inspector 3 for the South region Division of Oil and Gas, and I of a telephone conversation between he and Jeanie Schmelzer via e-mail. He alleges that Jeanie has no records of oil sold from the lease. 154 barrels of oil was the reported production for this well in the year 2010. | ||||
-2031322215 | 2008-01-17 | An inspection revealed that this well is lacking identification at the well and the tank battery (common). | ||||
259135706 | 2012-06-27 | Dikes have been built around tanks and around well head. There are two flow lines coming in to the tank battery as it is shared with the other well on the property (p#62338). Contaminated material has been removed from around well head. New electric service boxes have been installed on the site. | ||||
-571198833 | 2011-10-26 | Met with Christopher Eiben and Andy Thomas, inspected well site and tank battery. Andy Thomas will issue a Compliance Notice to company on violations and will also send Mr. Eiben a copy of Notice. | ||||
-586200007 | 2008-03-06 | A follow-up inspection revealed that the company has provided identification at the well (common tank battery). However, it was found that gas is being vented from the well without the use of a flare. | ||||
838035540 | 2011-10-26 | FOLLOW UP TO NOV # 1319737146 An inspection conducted with Dan Goins, Inspector 3 for the South region Division of Oil and Gas, presented three issues. There was oily material around well, well head did not have a dike, and gas was being vented from the well head. All oily material needs to be cleaned up around well site. Well head needs to have a dike contracted. A flare needs to be built compliant to 1501:9-9-05 (B). | ||||
-857151807 | 2012-06-27 | Accompanied Andy Thomas MRI 2 on complaint inspection. |
For data sources see[2]