X

Track changes made to this page

If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.



Privacy policy
Close this window

powered by ChangeDetection

34-173-61227

Well Details

Well ID: 34-173-61227
Loading map...
County: Wood
Municipality:
Operator Name: MARATHON ASHLAND PET. LLC
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date:
Unconventional: No
Configuration: Vertical
Well Status: Final Restoration
Violations: 0
Latitude: 41.41065037
Longitude: -83.74037865

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
1244558938 2009-06-08 Checked well. Gas is leaking from area where welding was done to attach well head control. Spoke to Mike Coyer by phone. He said he has tried to repair small leaks by welding and use of JB Weld material. The old casing is deteriorated and difficult to repair. Recommends clamping rubber sleeve around casing to help contain gas.
1244723622 2009-06-10 Met on site with Mike Coyer to repair gas leak on well. Jeff Fry also present during inspection. Village of Portage Fire Department assisted by supplying compressed air for Mike while making repair to well due to the serious health problems from H2S exposure while making repairs last time. A rubber gasket with steel clamp was placed around the weld area. This stopped the gas leak. In addition a 12 foot long PVC pipe was placed over the well and backfilled around the base. This will protect the well from vandalism and also vent gas above ground should the well start leaking again. These measures are only a temporary fix and the well needs to be properly plugged to eliminate the H2S gas problem. Members of the fire department on site confirmed that calls about gas leaking have occurred from this well. These calls not only reqired fire department response but also from the local gas company to try to find the source of the odor. The source of the gas was unknown at that time since the well was buried under a pile of rocks and debris.
1247516242 2009-07-13 Checked repairs made on well to stop H2S gas release. Gas odor is obvious standing down wind of riser pipe. Additional gas leaks are suspected from deteriorated casing on well. Will contact Jeff Fry and Mike McCormac about condition at well.
1247679612 2009-07-14 Checked well with Jeff Fry. There was some odor of gas but not as evident as on the previous day.
1267462787 2010-02-24 Bradner Oil, Marathon Oil and Total Safety on site to begin working on well . Total Safety monitoring for H2S gas around wellhead. Readings of H2S from well on previous sample were 1000 ppm. Fans placed around wellhead to dispurse gas from well. Gas bled off from well and temporary containment removed. Operator working on well was working with SCBA. Anybody on site required to where H2S detector and given safety briefing before entering site. Diverter head will be attached to well when temporary device removed.
1267546866 2010-03-02 Cement pumped into well on 3/1/10 set up at depth of 875 feet. There was approximately 75 feet of water on top of cement in well . Operator gravity poured 7 yards of 9 sack grout into well. Cement rose to surface of well with no fluids to surface. Bradner Oil, Marathon Oil and Total Safety on site for plugging.
1268835061 2010-03-03 Bradner Oil and Marathon employee Mondo on site removing equipment from site. Well cut off 4 feet below ground and ID plate attached. Cement to top of well casing.
1273753495 2010-05-10 Checked site for final reclamation. Area around well has not yet been final graded or seeded. Called Bob Harpster. He is aware site has not been completed. Conditions have been too wet to roto till area for seeding. Area will be roto tilled and seeded as soon as conditions allow.
1282748520 2010-08-25 Final restoration done.
1429951240 2010-02-25 Bradner Oil, Marathon Oil and Total Safety on site to continue to prepare well for plugging. Rotary drill set up over well. Bridge at top of well removed and well was flooded with brine to suppress gas. Gas monitoring done at wellhead before attaching diverter. Same safety precautions as on previous day except no SCBA required at wellhead.
-1955593454 2010-03-04 Equipment removed from site and area rough graded. Ground conditions muddy so final grading and seeding will be done when conditions improve.
486517203 2009-05-19 Area around well has been excavated to top of rock to expose well casing. Mike Coyer was on site and has welded control head on well. Valve installed on well to allow release of pressure before plugging. Gas pressure built up in well after being closed for a few minutes and flame burned 6-10 feet high.
-502871959 2010-03-01 Diverter succcesfully attached to well after some problems. Well was cleaned out to depth of 1133 feet. Several bridges were drilled through to reach total depth. Fluids in well suppressed gas so H2S not a problem. Operator pumped 126 sacks Class A cement into well. Fluids displaced to tank.. Cement will be allowed to set up over night and tag depth in morning. Bradner Oil, Marathon Oil and Total Safety on site.

For data sources see[1]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20.