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34-167-27324

Well Details

Well ID: 34-167-27324
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County: Washington
Municipality:
Operator Name: MADDEN VENTURES
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 1982-11-09
Unconventional: No
Configuration: Vertical
Well Status: Producing
Violations: 0
Latitude: 39.47863591
Longitude: -81.2900223

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
2004-0 585.0 0.0
2005-0 938.0 0.0
2006-0 1240.0 0.0
2007-0 1066.0 0.0
2008-0 382.0 0.0

For data sources see[1]

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
1058463836 2003-07-17 Inspection this day found well in violation of not having ID's, tank area looked good, dry, dike, well with pumpjack is producing. Will call operator tonight and give verbal warning regarding ID's. Will reinspect again in 1 month. Compliance Notice
1058463836 2003-07-17 Inspection this day found well in violation of not having ID's, tank area looked good, dry, dike, well with pumpjack is producing. Will call operator tonight and give verbal warning regarding ID's. Will reinspect again in 1 month. Compliance Notice
1058463836 2003-07-17 Inspection this day found well in violation of not having ID's, tank area looked good, dry, dike, well with pumpjack is producing. Will call operator tonight and give verbal warning regarding ID's. Will reinspect again in 1 month. Compliance Notice
-1111553839 2011-05-18 Talked with Joe Madden and he said would get back to me in a week with plans for the wells - talked like he would get money to Doug Admas and they would get wells back in production. Forwarded the information on to Doug Adams - told both parties that lease could be broken and they needed to be quick in their actions.
1156431018 2006-08-23 Re-inspect this day. Well producing with jack and valves look open but behind a locked fence so can't say for sure. Pipeline fittings out by road are disconnected and company won't turn production in so may not be producing. Tank has good ID's, good dike
1354027339 2012-11-27 Pending violation wrote 2/10 for idle well, still has not been resolved. Madden Ventures owns only 2 wells in Ohio and this well not producing, 2nd well (7323) has been idle for some time and landowner now has cancelled lease. Preparing to take legal action and should do both together. Call to this landowner, Mrs. Reynolds, to see status of lease found
1386546632 2010-02-04 My inspection this day found this well idle. This well is equipped with a pumping unit which does not appear to have worked for awhile. , jack has not been pumped, meter not turning. Doug Adams, pumper, reports well needs swabbed, has not been producing, can't get owner to pay bills. Plug or produce. Failure to comply may result in bond forfeiture. 5/18/2011 - Talked with Joe Madden this day - says will get back with me in a week with a plan for the wells - look for him to get them back in production, doesn't believe he has talked to the Armstrongs about selling them.
1397617865 2011-05-06 Inspection this day found no change, well still idle, valves shut on the well. Still has jack and other equipment, good ID's on tank and no dike. Tank and jack have 10' high fence around them. Landowner had called to enquire where the violation stood and what next step would be. Talked to Rob Armstrong and he says his sone Mike is buying the 2 wells - that attorney has all the information and documents getting drawn up for them (Armstrongs) to buy the wells. Talked to Virco and they verified that no gas sold from this well in over a year. No annual production since 2008.
242793203 2008-09-30 Operator says well producing - I say can't get into gate (10' fence) to verify. So he gives me a key but doesn't work - am able to squeeze thru opening, valves are just barely cracked. Meter in another location.. Will not resolve NOV until annual production turned in and it has not been yet.
-320829210 2008-11-14 Inspection found well is now producing, current chart in meter located at entirely different location, ID's up, annual production has been turned in to Columbus. Resolved.
-32368958 2010-02-04 FOLLOW UP TO NOV # 1386546632 My inspection this day found this well idle. This well is equipped with a pumping unit which does not appear to have worked for awhile. , jack has not been pumped, meter not turning. Doug Adams, pumper, reports well needs swabbed, has not been producing, can't get owner to pay bills. Plug or produce. Failure to comply may result in bond forfeiture. 5/18/2011 - Talked with Joe Madden this day - says will get back with me in a week with a plan for the wells - look for him to get them back in production, doesn't believe he has talked to the Armstrongs about selling them.
-402356595 2008-09-04 Inspection this day still found fence around tank and jack locked. Cannot get close enough to see alves but talked to landowner on property and she said well has not produced in year of more. I have asked repeatedly for company to turn in annual production but still have not. Electric meter has been removed - she said about a year ago, gas line above ground has been disconnected for many months. Well is idle. Good ID's.
-717016181 2005-02-07 Inspection this day found well with no ID's, tank is 210 bbl, all inside locked gate fence, appears to be producing but no annual production turned in - contacted pumper Doug Adams and asked to get ID's up and production in. Will give a couple weeks.
74547490 2011-12-20 My inspection today found the chart in the gas meter all wadded up and twisted. This chart has not been changed in long time (the date is not current and marking are faint). Well does not appear to be producing because the legible marks on the chart were registering zero.

For data sources see[2]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20. 
  2. "Ohio Department of Natural Resources RBDMS". [2]. 2015-06-19. Retrieved 2015-06-20.