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Well ID: 34-087-20275 | Loading map...
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County: Lawrence | |
Municipality: | |
Operator Name: CHESAPEAKE APPALACHIA LLC | |
Well Pad ID: | |
Farm/Lease Name: | |
First Permit Date: | |
Last Permit Date: | |
Spud Date: 1980-11-12 | |
Unconventional: No | |
Configuration: Vertical | |
Well Status: Final Restoration | |
Violations: 0 | |
Latitude: 38.50512903 | |
Longitude: -82.5507895 |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
---|---|---|---|---|---|---|
1985-0 | 0.0 | 0.0 | ||||
1986-0 | 0.0 | 0.0 | ||||
1987-0 | 0.0 | 0.0 | ||||
1989-0 | 0.0 | 0.0 |
For data sources see[1]
INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID | VIOLATION CODE | VIOLATION COMMENT |
---|---|---|---|---|---|---|
1097593289 | 2004-09-28 | Abandoned; disconnected and no ID. Picture #410. | Informal Letter | |||
1097593289 | 2004-09-28 | Abandoned; disconnected and no ID. Picture #410. | Compliance Notice | |||
-1165872660 | 2012-06-02 | Received E-mail from Rob Schindler Re: 6-1-12 they pulled all of the 5.5 casing out. There was a packer and swage on the bottom of the casing. They plan to check TD on 6-4-12 and set bottom plug on 6-5-12. | ||||
1220152590 | 2012-05-31 | Received E-mail from Rob Schindler Re: Ran cement bond log. Bottom of 5.5 was 1260'. The 5.5 is not cemented. | ||||
1316776327 | 2011-08-29 | No identification. Well must have identification(1509:9-9-05(A)(10): Well owner, lease name, well number, permit number, county, emergency telephone number. Well is equipped with swedge and master valve. Well is not connected to production equipment or production lines. There has been no recorded production. Submit production records per 1509.11. 1509.062 (A) Well must meet production requirements of one hundred thousand cubic feet of natural gas or fifteen bbls crude oil or combination thereof. If production is less, well shall be plugged or placed in temporary inactive well status. | ||||
1339091691 | 2012-05-21 | Chesapeake crew hot taped the 4.5 collar above the 4.5 by 5 swedge. 5 casing has 2 psi. Fluid level inside 5 casing at 492' from surface. Annulus has zero pressure. 5 annulus fluid level at 720' from surface. | ||||
-1598239107 | 2012-06-05 | Received E-mail from Rob Schindler Re: Tripped in hole to 2100'. Spotted 210 sacks cement with lost circulation material, through tubing. Tripped out of hole and waited on cement. Ran sand pump down and found top of cement at 1550'. Tripped tubing back to 1535' and pumped 110 sacks cement. Tripped tubing back out of hole. Plan to check top of cement in morning 6-6-12. | ||||
1844371319 | 2012-05-30 | Received E-mail from Rob Schindler Re: Checked TD at 2035'. Drilled with tools and sand pumped for 6 hours. Less than 1' of hole made. Got out a couple of gallons large shale caving. They are to run the cement bond log on 31st. | ||||
-2108846286 | 2011-12-19 | No identification. No change since last inspection. Well is not connected to production equipment or production lines. | ||||
-789276166 | 2012-06-06 | Tag top of cement plug at 1210'. Pumped gel spacer, Big Injun Plug and surface plug. Steel pits used during plug job. No earthen pits constructed. Viking well service rig and water truck. Superior Well Services Cement contractor. | ||||
-815283655 | 2012-07-05 | Location is graded. Good vegetative cover established. All equipment has been removed. |
For data sources see[2]