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34-089-24368

Well Details

Well ID: 34-089-24368
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County: Licking
Municipality:
Operator Name: ROYALTY ENTERPRISES INC
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 1982-01-13
Unconventional: No
Configuration: Vertical
Well Status: Producing
Violations: 0
Latitude: 40.05080933
Longitude: -82.32669936

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
1986-0 966.0 581.0
1987-0 907.0 507.0
1988-0 721.0 397.0
1989-0 653.0 311.0
1990-0 466.0 360.0
1991-0 116.0 326.0
1992-0 55.0 350.0
1993-0 523.0 302.0
1994-0 213.0 287.0
1995-0 195.0 228.0
1996-0 0.0 227.0
1997-0 0.0 256.0
1998-0 0.0 203.0
2000-0 0.0 185.0
2001-0 0.0 162.0
2002-0 0.0 151.0
2003-0 0.0 114.0
2004-0 0.0 105.0
2005-0 0.0 209.0
2006-0 0.0 143.0
2014-0 0.0 147.0 0.0 147.0

For data sources see[1]

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
-1000241485 2005-01-26 ID posted. Compliance Notice
-1000241485 2005-01-26 ID posted. Compliance Notice
1171993403 2007-02-20 I witnessed the plug back operations today. Formation Cementing performed the job to plug back this well to produce the Newberg. A 200 foot cement plug was set on the Clinton through tubing.
1172159686 2007-02-21 I witnessed the second attempt to plug off the Clinton. The 20 sack plug that was set yesterday was taken by the formation. Today, another 20 sack plug was spotted through tubing to plug off the Clinton. Brian with Formation cementing completed the job.
1285781065 2007-05-07 Jeff Fry and I inspected this well. The pump jack was running and they are producing the salt water brine from the Big Lime. A one inch line is running through the woods to the road were they are pumping straight into the trucks.
1380368778 2013-11-18 This inspection was conducted as a compliance notice follow-up. Inspection revealed identification has not been posted.
1399895948 2014-05-07 This inspection was conducted as a compliance follow-up. Royalty Enterprises Inc. has been issued a Chief's Order to stop operating on 4/28/2014. The well was equipped with a pumping unit and electric motor. The well was not pumping during inspection. The flow line valve was in the open position and the electric was on. This well operates on an automatice electric timer. Identification has not been posted at the well. A tanker truck was seen loading water at the tank battery. The time of inspection was approximately 2:15 pm.
34674173 2002-04-08 Inspection revealed No ID posted at the well head and/or the storage tanks. NOV to be issued this date. WEATNER CONDITIONS: Mostly cloudy and 55 degrees.
599557715 2013-05-07 This inspection was conducted as part of a standard production well status check. The well was equipped with a pumping unit and motor. The well was not pumping during inspection. Valves on the wellhead were open. The tank battery consist of (3) storage tanks and a gas separator. No identification was posted at the wellhead or tank battery. Company will need to post proper identification and notify inspector upon completion. Note- Entry Lat/Long: N 40.04799 W -082.32298

For data sources see[2]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20. 
  2. "Ohio Department of Natural Resources RBDMS". [2]. 2015-06-19. Retrieved 2015-06-20.