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Well ID: 34-121-22109 | Loading map...
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County: Noble | |
Municipality: | |
Operator Name: NORTHWOOD ENERGY CORP | |
Well Pad ID: | |
Farm/Lease Name: | |
First Permit Date: | |
Last Permit Date: | |
Spud Date: 2010-08-12 | |
Unconventional: No | |
Configuration: Vertical | |
Well Status: Producing | |
Violations: 0 | |
Latitude: 39.75827706 | |
Longitude: -81.50913437 |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
---|---|---|---|---|---|---|
1984-0 | 2836.0 | 0.0 | ||||
1986-0 | 1593.0 | 0.0 | ||||
1987-0 | 1587.0 | 0.0 | ||||
1988-0 | 967.0 | 0.0 | ||||
1990-0 | 132.0 | 0.0 | ||||
1991-0 | 823.0 | 0.0 | ||||
1992-0 | 602.0 | 0.0 | ||||
1993-0 | 596.0 | 0.0 | ||||
1994-0 | 534.0 | 0.0 | ||||
1995-0 | 487.0 | 0.0 | ||||
1996-0 | 255.0 | 0.0 | ||||
1997-0 | 614.0 | 0.0 | ||||
2000-0 | 0.0 | 0.0 | ||||
2001-0 | 0.0 | 0.0 | ||||
2002-0 | 0.0 | 0.0 | ||||
2003-0 | 0.0 | 0.0 | ||||
2004-0 | 0.0 | 0.0 | ||||
2005-0 | 160.0 | 0.0 | ||||
2006-0 | 456.0 | 0.0 | ||||
2007-0 | 143.0 | 0.0 | ||||
2008-0 | 0.0 | 0.0 | ||||
2009-0 | 0.0 | 0.0 | ||||
2010-0 | 0.0 | 0.0 | ||||
2011-0 | 0.0 | 0.0 | ||||
2012-0 | 0.0 | 0.0 | ||||
2013-0 | 0.0 | 0.0 | ||||
2014-0 | 0.0 | 0.0 | 0.0 | 0.0 |
For data sources see[1]
INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID | VIOLATION CODE | VIOLATION COMMENT |
---|---|---|---|---|---|---|
1281884187 | 2010-08-13 | Company rep called and stated they were moving service rig in on site to possibly repair well, they suspect casing has hole in it and they might want to possibly plug well back to Ohio Shale told them to apply for plug back permit ASAP. | ||||
1552059902 | 2014-11-19 | My inspection today finds the well has been plugged back. The well is equipped with tubing and rods and is awaiting a pump jack to be set. The tank battery has yet to be built. The pit that was used for the plug back has been filled in and the surface has been rough graded. | ||||
-1608673291 | 2010-08-16 | On site to witness perf job on casing in preparation for plugback operation. | ||||
1773646201 | 2014-07-14 | The well has been sold to Northwood Energy. I spoke to Bill Arnholt with Northwood Energy about the well on 7-11-2014. Mr. Arnholt stated that the company would be recompleting the well in the next few weeks and returning it to production. | ||||
1858441776 | 2012-02-27 | Upon inspection of well site found the plug back pit filled and vegetation established, at well head the following equipment is present 8.625 surface casing, 4.5 production casing, 1.5tubing with the well being produced by the means of a pumping unit, inspector will note only the tubing and surface casing are hooked up at this time 4.5 production casing is not hooked up, 100 barrel tank on well site also. | ||||
2018862229 | 2014-03-18 | My inspection finds the well is equipped to be produced by a pump jack. The casing valves are shut. The tank battery is comprised of one 100 bbl tank located in a dike. A separator is located out of the dike with the inlet valve closed. The owner has reported zero production on the well since 2007. THE WELL SHALL BE PLUGGED WITHIN 180 DAYS. | ||||
368868607 | 2014-09-23 | My inspection today finds Northwood Energy is preparing to perform hydraulic stimulation on the well and return it to production soon after. | ||||
9481758 | 2014-07-31 | My inspection today finds Davis Well Service has pulled the tubing and rods out of the well and they are now attempting to pull the casing out of the well. The casing is hung in the hole. |
For data sources see[2]