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34-153-20865

Well Details

Well ID: 34-153-20865
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County: Summit
Municipality:
Operator Name: MOORE WELL SERVICES INC
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 1980-08-13
Unconventional: No
Configuration: Vertical
Well Status: Plugged and Abandoned
Violations: 0
Latitude: 41.16797128
Longitude: -81.53531555

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
1984-0 8621.0 252.0
1985-0 6553.0 169.0
1986-0 5024.0 188.0
1987-0 4193.0 134.0
1988-0 3920.0 118.0
1989-0 2287.0 135.0
1990-0 2180.0 85.0
1991-0 1940.0 69.0
1993-0 2382.0 57.0
1994-0 1188.0 151.0
1995-0 569.0 66.0
1996-0 531.0 0.0
1998-0 0.0 0.0
1999-0
2000-0 0.0 0.0
2001-0 0.0 0.0
2002-0 0.0 0.0
2003-0 0.0 0.0
2004-0 0.0 16.0
2005-0 0.0 16.0
2006-0 0.0 0.0
2007-0 0.0 0.0

For data sources see[1]

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
1184958097 2007-07-13 Medina Supply delivered and placed five cubic yards of 9 sack grout in the 8-5/8 casing. The grout came to surface before falling back down hole. The plan now is top the hole off with bentonite hole plug and quikrete cement.
-1194606880 2007-07-11 The well has been plugged and abandoned. The violation is corrected.
-1685034826 2003-03-31 The well is still idle. There have been no complaints and neither the well nor the tank battery are leaking. Bob Moore stated that he has been waiting for a swab rig to work on this well.
18179570 2002-07-26 Status check inspection. The last reported production from this well was in 1998. The well needs to either be placed back into production or properly plugged and abandoned.
-293731643 2007-07-16 Moore placed 48 sacks of bentonite hole plug topped with 4 sacks of Quikrete into the 8-5/8 casing to complete the plug job.

For data sources see[2]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20. 
  2. "Ohio Department of Natural Resources RBDMS". [2]. 2015-06-19. Retrieved 2015-06-20.