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34-087-20309

Well Details

Well ID: 34-087-20309
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County: Lawrence
Municipality:
Operator Name: SMITH RONALD DBA CHIPCO
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 1981-12-14
Unconventional: No
Configuration: Vertical
Well Status: Final Restoration
Violations: 0
Latitude: 38.50849912
Longitude: -82.58417842

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
1985-0 0.0 0.0
1986-0 0.0 0.0
1987-0 0.0 0.0
1988-0 0.0 0.0
1993-0 0.0 0.0
1994-0 0.0 0.0
1995-0 0.0 0.0
1997-0 0.0 0.0
1998-0 0.0 0.0
1999-0 0.0 0.0
2000-0 0.0 0.0
2001-0 0.0 0.0
2002-0 0.0 0.0
2003-0 0.0 0.0
2004-0 0.0 0.0
2009-0 0.0 0.0

For data sources see[1]

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
1114639703 2011-08-24 Ran tools hit solid at 2400'. Ran 2375' 1.5tubing. Pump cement plug through tubing. 58 sks. Informal Letter
1114639703 2011-08-24 Ran tools hit solid at 2400'. Ran 2375' 1.5tubing. Pump cement plug through tubing. 58 sks. Phone Call
1240494471 2009-04-23 Talked to Chip Smith (well owner) today at 9:42 am. We discussed the Idle well violations on his wells. He took over the wells to plug them for salvage. Chip told me that he is working a deal with North Coast Energy to plug some of their wells also. He plans to start plugging as soon as it dries out. I told chip that I had not seen any plug permits issued for his wells. He said that the permits will be filled with in a week.
1314290150 2011-08-25 Witnessed surface plug. 100 feet of class A inside 8 5/8 casing. 2% gel mix 1.36 yield, 14.7#.
-1484913536 2004-10-01 No ID; disconnected from line; abandoned.
-1657831826 2011-08-29 Pit filled in. Site graded. Dozer on location.
-1746989338 2009-03-16 No identification. Wellhead not connected to any production equipment or lines. Valves are closed. Land owner said that well has never been in production. RBDMS production records show 0 production from 1985 to 2004. No production records have been submitted from 2005 to present. Chipco took ownership in 2005. Well needs Identification. Well must be capable of commercial production or plugged. Production records need to be submitted for 2005 to present.
711676516 2011-12-19 Site is graded. Good vegetative cover established. No equipment on location.
PL14139 Preliminary Restoration done information from Data Point

For data sources see[2]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20. 
  2. "Ohio Department of Natural Resources RBDMS". [2]. 2015-06-19. Retrieved 2015-06-20.