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34-053-20997

Well Details

Well ID: 34-053-20997
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County: Gallia
Municipality:
Operator Name: CONTINENTAL RESOURCES INC
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 2008-06-22
Unconventional: No
Configuration: Vertical
Well Status: Final Restoration
Violations: 0
Latitude: 38.74864919
Longitude: -82.30621731

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
2008-0 0.0 0.0

For data sources see[1]

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
-1009898814 2009-07-10 Pumped 1st plug on 7-9-09 from 2885' to 2485'. On 7-10-09 ran back to 2885' and did not tag plug. Pump LCM and fresh water and try to achieve circulation. Took 80 bbls to circulate to surface. Pump 20 bbls. Stop circulation then re start took 120 bbls total. Pumped plug from 2885' to 2485'. Ran tubing back to try and tag TOC was unable ran tubing back to 2885' and pumped another plug from 2885' to 2485'. WOC. Compliance Notice
1016848316 2014-12-04 Preliminary Restoration requirements met.
1197458774 2008-10-30 Carper Well Service Rig is swabbing on the well. Talked to Shannon Stevens on location about the pit and timelines for restoration. Pit is open. Pit liner is in good shape, no tears in lining.
1214311722 2008-06-23 Surface cement job. I arrived on location and the rig crew was still trying to get the 9 5/8 in the hole. They were having trouble with the threads and there was a slight bend in the casing which was causing it to cross thread. They hit mud and decided to drive 20 to 41' then drill 17 1/2 hole 63' for the 13 3/8 conductor. Then a 12 1/4 hole was drilled to 645'. They were going to set 617' of 9 5/8 but due to the cross threading problem they set 573' of 9 5/8. I approved the change to the casing program in the field. A 1/4 stream of water was hit at 350'. A basket was set at 256'. The well had good circulation and good cement returns to the surface.
1241793261 2009-05-07 Spud date 6-22-08, Restoration due 3-22-09. Site is rutted with standing water. No attempt to vegetate site. Site is bare ground. No identification on well. Well is equipped with a pump jack, tubing, rods, and a flare. Flare is not connected at this time. Robert Stonerock (South Region Supervisor) accompanied me on the inspection. A pool of oil around the wellhead 3 feet in diameter. I called Merl Richards (company representative) at 6:18 pm on 5-7-09 and informed him of the violations.
1262110754 2009-05-13 No identification. Well is equipped with a flare set 95' from the well. Site is rutted and the soil is bare. No effort has been made to restore the site. Wellhead has a 3' pool of oil around it. Well is equipped with tubing, rods, pump jack, and gas motor.
-1502129735 2008-11-12 Leaking gas around the back side of the 7. Gas is bubbling up through a puddle at the surface. Can hear gas leak but it doesn't show up on the gas detector. I? Have talked to Jimmy Ray about this well.
1526835060 2009-07-07 Cut the 4.5 casing at 2743' MD. Pulled to 2690' and swabbed the well. Fluid level at 1000'. Swabbed again and it kicked off.
-1673355379 2010-02-03 Site is graded. Have established good vegetative cover on location. Landowner will use site for hay field. Gravel pile has been left at request of landowner.
-1717658445 2008-07-14 Pit had to be relined due to a tear. An un determined amount of fluid was lost from the pit. They are preparing to log the hole. Then plug it back to drill horizontally.
1731249331 2008-06-27 I received a call from Merl Richards and he informed me that the rig had a brine leak at their mud pump. I met Merl on location and we discussed the clean up procedures. The brine is contained in the clay soil and is pooled up in 3 areas 1.5' by 6', 3' by 2 ' and 2' by 5' all pools were less than 2 deep. The leak was caused by a leaking union on the mud pump. I told Merl to contain the soil and to dispose of it in the pit during restoration.
203935771 2009-07-15 Solidify pit with 140 sks cement. Mix with track hoe.
225610146 2008-07-15 Straight hole TD is 2915'. Core samples have been taken and the hole has been logged. Plug back from 2915' to 2050'. This is to be used for a kick plug during the horizontal portion of the well. The pit liner had to be replaced again due to a tear. I witnessed the liner being installed. And was able to witness the plug back at the same time.
-389346228 2008-12-19 A slight bubbling was noticed at the wellhead. Bubbles 1/4 inch in diameter. I took a video. All valves on the wellhead are shut off. My gas detector did not show any explosive levels of gas at the wellhead. There was a good breeze at the time of inspection.
-586192040 2008-06-19 GPS on the well stake. Site is being built now. They are building a gravel entrance and will stone most of the location. This is an horizontal well. The same crew that did the Richfield wells is doing this well. Merl Richards, Jimmy Ray and the SW Jack rig # 8.
881545284 2008-08-03 Well has been drilled and is making 500psi naturally. Horizontal portion of the well is in the Rhine Street 2722' to 2793'. Updated well GPS location. Drill pit is in good shape and is being currently used for drilling the 996. No violations observed during inspection.

For data sources see[2]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20. 
  2. "Ohio Department of Natural Resources RBDMS". [2]. 2015-06-19. Retrieved 2015-06-20.