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34-055-22101

Well Details

Well ID: 34-055-22101
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County: Geauga
Municipality:
Operator Name: WILKES ENERGY INC
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 2009-08-23
Unconventional: No
Configuration: Vertical
Well Status: Producing
Violations: 0
Latitude: 41.41707501
Longitude: -81.03048291

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
2009-0 0.0 0.0
2010-0 6188.0 517.0
2011-0 9279.0 502.0
2012-0 4910.0 311.0
2013-0 4276.0 298.0
2014-0 5004.0 365.0 259.0 365.0

For data sources see[1]

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
1251128152 2009-08-24 Rig moved from permit 22100 to permit 22101 today. Pits are under construction, hard clay appears to be the soil type. Lease road is stable. Site is stable.
1289249606 2010-11-08 Well is a pump jack well. Lease road is stable. Tank battery dike is in good repair. Two 110Bbl, a half tank in the battery and a mechanical separator. Identification sign is posted on the battery. Well site is in good repair. Affected area has been graded, seeded and vegetation is established.
-1691062128 2013-03-25 The well is equipped with a pump jack. The tank battery and well are in good repair. The tank battery consists of two 100 BBL production tanks, a 50 BBL brine tank, and a mechanical separator. The proper identification is located on the tank battery. The lease road is in stable condition. The tank battery and lease road is being shared with permit # 2-2100.
1945392410 2009-08-25 Site is stable. Lease road is stable. Pits are in good repair. On site for surface cement. Pipe was new R-3 20lb pipe. Good circulation, no lose of circulation during drilling. Operator broke circulation and ran 5 gel and flake ahead. Ran 65 sacks of light cement ahead, then 85 sacks of Class A. 15 BBL return of cement to surface. Cement held at surface. CND was waived on this site, shale was at 16 feet. Driller had good cutting samples, taken every 5 feet.
-275414003 2012-08-16 My inspection today found a pumping unit well. The 8.625 annulus on the well was open. The tank battery had two 140bbl production tanks and a mechincal separator. The tank battery, tank battery dike and lease road were in good repair.
-830433122 2009-09-09 Service rig on site. Pits have been filled. Drainage controls are in place.
-898425852 2009-10-22 Pits have been filled in. Site is stable, drainage controls are in place. Well is going to be a pump jack well when it is put on line. Seeding is taking hold.

For data sources see[2]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20. 
  2. "Ohio Department of Natural Resources RBDMS". [2]. 2015-06-19. Retrieved 2015-06-20.