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34-111-24444

Well Details

Well ID: 34-111-24444
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County: Monroe
Municipality:
Operator Name: ANTERO RESOURCES CORPORATION
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 2013-12-27
Unconventional: No
Configuration: Vertical
Well Status: Producing
Violations: 0
Latitude: 39.83291198
Longitude: -81.30203577

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
2014-4 580212.0 38.0 11.0 38.0
2015-1 1131113.0 90.0 207.0 90.0

For data sources see[1]

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
1064294239 2014-03-31 Status check inspection on the drilling process found Patterson 342 drilling rig on location drilling the 12.250 borehole at a depth of 2,480', the company is running a gyro survey.
-1165376058 2014-04-10 On 04/08/14 I was notified by the company man that the 9.625 cement job locked up during displacement and they would be drilling out the cement and bond logging to find the top of cement (TOC). On 04/09/ 14 the TOC was tagged at 1,550' and the remainder of the cement began to be drilled out down to the casing float collar. On 04/10/14 the hole was bond logged and a solid bridge plug set in the 9.625 casing at 4,515' and the casing perforated from 4,502' to 4,498' with 16 perforations, circulation was then broke and the hole circulated bottoms up 4 times, a cement retainer was then set and the drill string stung into the retainer and the casing cement squeeze job applied by Allied Cement services using 1594 sacks of Class A cement with a 15.6# weight and 1.8 yield with no additives and 50% cement excess ran with no cement returns to surface. The cement retainer and bridge plug shall be drilled out and the well bond logged.
1390841073 2014-01-27 Status check inspection on the drilling progress found the current well 24 bore surface hole has been drilled to a depth of 418', the company is running a borehole deviation survey and will then condition the hole in preparation to run the 18.625 surface casing.
1391050869 2014-01-28 On 01/28/14 Falcon Drilling rig # 20 is now on the hole and 418' of 18.625 surface casing was set and cemented to surface using 850 sacks of class A 2% calcium 1/4 pps flake with cement returns to surface @ 70 barrels into total displacement, the cement weight was verified at 15.6# and the mix water checked for chlorides, the total job on site time was 10 hours due to the -20 degree temperatures.
1391525554 2014-02-04 On 02/04/14 the 1st intermediate casing string was set and cemented to surface by Allied Cement services using 1841 sacks of class A- 2% calcium-1/4# flake cement with 80 barrels of cement returns to surface and the plug landed at 890 psi followed by the casing being pressure tested to 1410 psi with no recorded pressure loss.
1396551055 2014-04-03 Status check inspection of the drilling process found Patterson Drilling rig 342 drilling the 2nd intermediate 12.250 borehole on air at a depth of 4,227' with a projected total depth of 6,900'.
1397266353 2014-04-11 Notification was received from the company rig supervisor James Harvey that the 9.625 remedial squeeze job that we initiated the previous night was being bond logged and a top of cement was indicated at 2,400' with several cement stringers up the hole into the bottom of the 13.375 previously set casing string at 2,100'. We will meet on location and review all records and logs on the next working day, the drilling rig will skid to drill the 2nd intermediate on the next well on the pad. Notification was made to my supervisor Brent Bear and further remediation work will not be required.
1402326745 2014-06-09 Status check inspection found the well bore total drilling depth has been reached at 16,311' using a 8.5 diameter drill bit with a directional azimuth in the horizontal section of 151.16 degrees.
1415664582 2014-11-10 Status check on the well completion process found Fortis Well Service work over rig on the hole rigging up to drill out the stimulation completion wireline plugs. A proper functioning work over blow out preventer is in place and has been function tested and charted.
1426378065 2015-02-09 Preliminary Restoration status check inspection found the well is now in production with a gas processing unit in place on location associated to the said well. There a quantity of 8- 400 barrel production tanks on location supporting the 6 producing wells now located on the well pad. Preliminary Restoration was passed on this day.
1578916499 2014-02-03 Status check inspection to witness the running of the 13.375 1st intermediate well bore casing string set at a depth of 2,180' total casing with a 17.5 well bore total depth of 2,177'. A casing tally was received and the company will call when the cementer arrive on location.
1597411347 2014-08-25 Status check inspection of the well pad post stimulation found the company men on site and the old containment has been removed and the location is being leveled in preparation of installing new containment prior to commencing stimulation, a suggestion was made to improve the well pad site containment in the area behind the fluid separators.
-173512450 2014-05-30 Status check inspection on the current drilling progress found the current drilling depth to be 12,328' in the horizontal well bore section using 14.7# oil based drilling mud with no recorded fluid losses and a current directional azimuth of 149 degrees.
-211604977 2014-04-09 Notification was received on 04/09/014 from the company man on site that during the cementing of the 9.625 2nd intermediate well bore section that the casing pressured up during cement displacement, upon inspection on this day I was notified that the top of the cement inside the 9.625 casing was at 1550' and the estimated top of cement on the annular side was approximately 3,300' and once the company finished drilling out the cement from the inside the casing a bond log shall be ran and the cement job repaired accordingly.
-3932550 2013-12-27 The said well was spudded on this day by Express services wit 100' of 26 conductor to be set in a 32 borehole.

For data sources see[2]

Chemical Data

HF Fluid Concentration Ingredient Additive Concentration Trade Name Purpose CAS number Supplier
0.0027 Deionized Water 28.0 K-BAC 1020 LLC 7732-18-5 U.S. Well Services
20.0 2 10222.0 K-BAC 1020 LLC 2-dibromo-3-nitrilop U.S. Well Services
0.004 Anionic Copolymer 0.0 SI-1000 LLC Proprietary U.S. Well Services
0.00302 Water 30.0 SI-1000 LLC 7732-18-5 U.S. Well Services
0.00362 Ethylene Glycol 20.0 SI-1000 LLC 107-21-1 U.S. Well Services
0.00043 Diethylene Glycol 30.0 AI-301 Acid Corrosion Inhibitors 111-46-6 U.S. Well Services
0.00034 Methenamine 20.0 AI-301 Acid Corrosion Inhibitors 100-97-0 U.S. Well Services
0.00013 Polyethylene polyamine 10.0 AI-301 Acid Corrosion Inhibitors 68603-67-8 U.S. Well Services
0.00015 Hydrogen Chloride 10.0 AI-301 Acid Corrosion Inhibitors 7647-01-0 U.S. Well Services
0.00373 Ethoxylated alcohol blend 5.0 WFRA-405 LLC Proprietary U.S. Well Services
0.02986 Water 40.0 WFRA-405 LLC 7732-18-5 U.S. Well Services
0.02404 Petroleum Distillates 22.0 WFRA-405 LLC 64742-47-8 U.S. Well Services
0.09809 Water 87.5 HCL Acid (12.6%-18.0%) LLC 7732-18-5 U.S. Well Services
0.02343 Hydrogen Chloride 18.0 HCL Acid (12.6%-18.0%) LLC 7647-01-0 U.S. Well Services
0.00225 Ammonium Persulfate 100.0 AP One LLC 7727-54-0 U.S. Well Services
88.9148 Water 100.0 Water Base Fluid 7732-18-5 Antero Resources
0.08809 Guar Gum 50.0 LGC-15 LLC 9000-30-0 U.S. Well Services
0.01347 Suspending agent (solid) 3.0 LGC-15 LLC 14808-60-7 U.S. Well Services
0.00529 Surfactant 3.0 LGC-15 LLC 68439-51-0 U.S. Well Services
0.08343 Petroleum Distillates 60.0 LGC-15 LLC 64742-47-8 U.S. Well Services
100.0 Crystalline Silica 14808.0 Sand LLC quartz U.S. Well Services

For data sources see[3]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20. 
  2. "Ohio Department of Natural Resources RBDMS". [2]. 2015-06-19. Retrieved 2015-06-20. 
  3. "FracFocus Chemical Disclosure Registry". [3]. 2015-08-10. Retrieved 2015-08-10.