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37-129-27814

Well Details

Well ID: 37-129-27814
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Operator Name: HUNTLEY & HUNTLEY INC
First Permit Date: 2009-02-09
Last Permit Date: 2009-02-09
Spud Date: 2009-08-11
Unconventional: No
Horizontal: No
Violations: None
Latitude: 40.331437
Longitude: -79.759119

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
2013-0 11571.67 365.0 0.0 0.0 0.0 0.0
2012-0 17260.0 366.0 0.0 0.0 0.0 0.0
2011-0 21044.0 365.0 0.0 0.0 0.0 0.0
2010-0 23700.0 365.0 0.0 0.0 0.0 0.0
2009-0 441.0 30.0 0.0 0.0 0.0 0.0

Waste Data

PERIOD TYPE QUANTITY UNITS DISPOSAL METHOD WASTE FACILITY PERMIT ID WASTE FACILITY NAME FACILITY CITY FACILITY STATE
2012-0 PRODUCED FLUID 70.0 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE PA0254185 RESERVED ENVIRONMENTAL SERVICES MOUNT PLEASANT PA
2009-0 DRILLING FLUID WASTE 1770.0 Bbl PUBLIC SEWAGE TREATMENT PLANT PA0026913 MCKEESPORT SEWAGE TREATMENT PLANT MCKEESPORT PA
2009-0 DRILLING FLUID WASTE 160.0 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE PA0091472 TUNNELTON LIQUIDS COMPANY SALTSBURG PA
2010-0 DRILLING FLUID WASTE 951.0 Bbl PUBLIC SEWAGE TREATMENT PLANT PA0026913 MCKEESPORT SEWAGE TREATMENT PLANT MCKEESPORT PA
2010-0 FRACING FLUID WASTE 85.0 Bbl PUBLIC SEWAGE TREATMENT PLANT PA0026913 MCKEESPORT SEWAGE TREATMENT PLANT MCKEESPORT PA
2010-0 DRILLING FLUID WASTE 110.0 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE PA0091472 TUNNELTON LIQUIDS COMPANY SALTSBURG PA
2010-0 PRODUCED FLUID 80.0 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE PA0091472 TUNNELTON LIQUIDS COMPANY SALTSBURG PA
2011-0 PRODUCED FLUID 80.0 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE PA0095273 PA BRINE TRT INC - JOSEPHINE PLT, INDIANA COUNTY JOSEPHINE PA
2012-0 PRODUCED FLUID 70.0 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE PA0254185 RESERVED ENVIRONMENTAL SERVICES MOUNT PLEASANT PA
2013-0 PRODUCED FLUID 100.0 Bbl CENT WASTE TRT FAC NPDES DISCHARGE PA0095273 FLUID RECOVERY SERVICE JOSEPHINE FACILITY JOSEPHINE PA

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID
1821665 2009-08-12 No Violations Noted US ENERGY DRILLING FOR HUNTLEY, I ARRIVE ON LOCATION WITH MIKE ARCH, FOUND ACCESS ROAD IN BAD SHAPE, PIT WALLS ARE STRAIGHT UP AND DOWN WITH NO FENCE AROUND PIT. E&S PLAN IS NOT SITE SPECIFIC. ERIC FINDLEY AGREED TO TAKE CARE OF ISSUES. I WILL RETURN TOMORROW TO OBSERVE PROGRESS
1821679 2009-08-18 No Violations Noted US ENERGY RIGGED BACK UP TO DRILL. HUNTLEY DECIDED NOT TO PRODUCE THE OPEN FLOW AT 1410. THEY CONTINUED TO DRILL UNTIL THEY HIT 100GPM, NOW THEY HAVE WATER TRUCKS RUNNING CONSTANTLY TO KEEP UP WITH THE WATER. FINDLEY SAYS HE CAN SUBSTITUTE HIS BOP AS A DIVERTER ONLY WITHOUT VOLATING 78.72. I INTERPRET THIS PASSAGE TO MEAN THAT A BOP STACK MAY NOT BE ATTACHED TO ANY LESS THAN 400' REGARDLESS OF INTENTION TO USE OR NOT
1821687 2009-08-13 No Violations Noted US ENERGY DRILLED TO 1922, SMELLED GAS BUT DID NOT REALIZE UNTIL THEY WERE TRIPPING OUT, HOW MUCH GAS THEY HAD. SUPERIOR WAS ON SITE LOGGING THE WELL WHEN I ARRIVED. DAVE JANCO & ERIC FINDLEY WERE ALSO ON LOCATION. THEY HIT 1/2 MILLION OPEN FLOW, HAVE CEASED DRILLING AND DETERMINED THE GAS TO BE COMING FROM 1410 FROM THE LOYALHANNA. ERIC HAS 1400' OF 4.5 ON IT'S WAY FROM MCJUNKEN AND AN 8 5/8-4.5 PACKER ON ROUTE FROM BIG JOHN AT MILLER'S. THEY ARE MOVING OUT THE RIG, MOVING IN A SERVICE RIG AND SETTING THE 4.5 ON A PACKER TO TAKE THE PRESSURE OFF THE 9 5/8. THEIR PLAN IS TO CLOSE IN AND MONITOR THE ANNULUS OUTSIDE THE 4.5 AND PUT IT INTO THEIR LINE (30LBS) AND PRODUCE LOYALHANNA GAS FROM 1410 WITH RATHOLE TO 1922. THEY PLAN TO APPLY FOR A 1000' VERTICAL VARIANCE, SKID ADN DRILL ANOTHER WELL NEXT TO THIS WELL, CEMENTING CASING IN FROM 2410 UP AND HAVE AGREED TO CEMENT CASING IN AT 400 ON THE NEXT WELL SO THEY CAN USE THEIR BOP IF THEY TAKE ANOTHER GAS KICK. THEIR E&S PLAN HAS BEEN UPDATED PITS ARE FENCED IN, ACCESS ROAD HAS MORE LIMESTONE
1870167 2010-02-04 No Violations Noted PRODUCING WELL, OPEN PIT, FENCE IS FALLING DOWN AND PARTIALLY MISSING. ANNULUS IS CLOSED, SITE HAS NOT YET BEEN RESTORED.

References