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Well ID: 37-129-27814 | Loading map...
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Country: United States | |
State: Pennsylvania | |
County: Westmoreland | |
Municipality: North Huntingdon Township | |
Operator Name: HUNTLEY & HUNTLEY INC | |
Well Pad ID: | |
Farm/Lease Name: WILLOW GLENN 81-3 | |
License Status: | |
Spud Date: | |
Permit Date: 2009-02-09 | |
Well Type: GAS | |
Unconventional Well: N | |
Configuration: Vertical Well | |
Conservation: No | |
Latitude: 40.331438 | |
Longitude: -79.759119 |
Date | Event |
---|---|
2009-02-09 | New Permit Application |
2009-08-11 | Performed Spud Operation |
2009-08-20 | Drilling Completion |
2009-12-15 | Perforation |
2013-05-31 | NEWLY DRILLED |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Gas Production Days | Oil Quantity (bbl) | Oil Production Days | Water Quantity (bbl) | Water Production Days |
---|---|---|---|---|---|---|---|
2009 | HUNTLEY & HUNTLEY INC | 441.00 | 30 | 0.00 | 0 | 0.00 | 0 |
2010 | HUNTLEY & HUNTLEY INC | 23,700.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2011 | HUNTLEY & HUNTLEY INC | 21,044.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2012 | HUNTLEY & HUNTLEY INC | 17,260.00 | 366 | 0.00 | 0 | 0.00 | 0 |
2013 | HUNTLEY & HUNTLEY INC | 11,571.67 | 365 | 0.00 | 0 | 0.00 | 0 |
2014 | HUNTLEY & HUNTLEY INC | 11,455.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2015 | HUNTLEY & HUNTLEY INC | 9,629.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2016 | HUNTLEY & HUNTLEY INC | 7,705.00 | 366 | 0.00 | 0 | 0.00 | 0 |
2017 | HUNTLEY & HUNTLEY INC | 6,102.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2018 | HUNTLEY & HUNTLEY INC | 7,145.00 | 365 | 0.00 | 0 | 0.00 | 0 |
2019 | HUNTLEY & HUNTLEY INC | 7,125.00 | 365 | 0.00 | 0 | 0.00 | 0 |
For data sources see[5]
Period | Operator | Waste Type | Quantity | Disposal Method | Waste Facility ID |
---|---|---|---|---|---|
2009 | HUNTLEY & HUNTLEY INC | Drilling Fluid Waste | 160.00 Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | PA0091472 |
2009 | HUNTLEY & HUNTLEY INC | Drilling Fluid Waste | 1,770.00 Bbl | PUBLIC SEWAGE TREATMENT PLANT | PA0026913 |
2010 | HUNTLEY & HUNTLEY INC | Fracing Fluid Waste | 85.00 Bbl | PUBLIC SEWAGE TREATMENT PLANT | PA0026913 |
2010 | HUNTLEY & HUNTLEY INC | Produced Fluid | 80.00 Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | PA0091472 |
2010 | HUNTLEY & HUNTLEY INC | Drilling Fluid Waste | 110.00 Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | PA0091472 |
2010 | HUNTLEY & HUNTLEY INC | Drilling Fluid Waste | 951.00 Bbl | PUBLIC SEWAGE TREATMENT PLANT | PA0026913 |
2011 | HUNTLEY & HUNTLEY INC | Produced Fluid | 80.00 Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | PA0095273 |
2012 | HUNTLEY & HUNTLEY INC | Produced Fluid | 70.00 Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | PA0254185 |
2013 | HUNTLEY & HUNTLEY INC | Produced Fluid | 100 Bbl | CENT WASTE TRT FAC NPDES | PA0095273 |
2013 | HUNTLEY & HUNTLEY INC | Produced Fluid | 100.00 Bbl | CENT WASTE TRT FAC NPDES DISCHARGE | PA0095273 |
2017 | HUNTLEY & HUNTLEY INC | Produced Fluid | 25.00 Bbl | CENT WASTE TRT FAC NPDES DISCHARGE | PA0095273 |
2018 | HUNTLEY & HUNTLEY INC | Produced Fluid | 20.00 Bbl | CENT WASTE TRT FAC NPDES DISCHARGE | PA0095273 |
For data sources see[6]
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
1821665 | Primary Facility | 2009-08-12 | Drilling/Alteration | No Violations Noted | US ENERGY DRILLING FOR HUNTLEY, I ARRIVE ON LOCATION WITH MIKE ARCH, FOUND ACCESS ROAD IN BAD SHAPE, PIT WALLS ARE STRAIGHT UP AND DOWN WITH NO FENCE AROUND PIT. E&S PLAN IS NOT SITE SPECIFIC. ERIC FINDLEY AGREED TO TAKE CARE OF ISSUES. I WILL RETURN TOMORROW TO OBSERVE PROGRESS |
1821679 | Primary Facility | 2009-08-18 | Drilling/Alteration | No Violations Noted | US ENERGY RIGGED BACK UP TO DRILL. HUNTLEY DECIDED NOT TO PRODUCE THE OPEN FLOW AT 1410. THEY CONTINUED TO DRILL UNTIL THEY HIT 100GPM, NOW THEY HAVE WATER TRUCKS RUNNING CONSTANTLY TO KEEP UP WITH THE WATER. FINDLEY SAYS HE CAN SUBSTITUTE HIS BOP AS A DIVERTER ONLY WITHOUT VOLATING 78.72. I INTERPRET THIS PASSAGE TO MEAN THAT A BOP STACK MAY NOT BE ATTACHED TO ANY LESS THAN 400' REGARDLESS OF INTENTION TO USE OR NOT |
1821687 | Primary Facility | 2009-08-13 | Drilling/Alteration | No Violations Noted | US ENERGY DRILLED TO 1922, SMELLED GAS BUT DID NOT REALIZE UNTIL THEY WERE TRIPPING OUT, HOW MUCH GAS THEY HAD. SUPERIOR WAS ON SITE LOGGING THE WELL WHEN I ARRIVED. DAVE JANCO & ERIC FINDLEY WERE ALSO ON LOCATION. THEY HIT 1/2 MILLION OPEN FLOW, HAVE CEASED DRILLING AND DETERMINED THE GAS TO BE COMING FROM 1410 FROM THE LOYALHANNA. ERIC HAS 1400' OF 4.5 ON IT'S WAY FROM MCJUNKEN AND AN 8 5/8-4.5 PACKER ON ROUTE FROM BIG JOHN AT MILLER'S. THEY ARE MOVING OUT THE RIG, MOVING IN A SERVICE RIG AND SETTING THE 4.5 ON A PACKER TO TAKE THE PRESSURE OFF THE 9 5/8. THEIR PLAN IS TO CLOSE IN AND MONITOR THE ANNULUS OUTSIDE THE 4.5 AND PUT IT INTO THEIR LINE (30LBS) AND PRODUCE LOYALHANNA GAS FROM 1410 WITH RATHOLE TO 1922. THEY PLAN TO APPLY FOR A 1000' VERTICAL VARIANCE, SKID ADN DRILL ANOTHER WELL NEXT TO THIS WELL, CEMENTING CASING IN FROM 2410 UP AND HAVE AGREED TO CEMENT CASING IN AT 400 ON THE NEXT WELL SO THEY CAN USE THEIR BOP IF THEY TAKE ANOTHER GAS KICK. THEIR E&S PLAN HAS BEEN UPDATED PITS ARE FENCED IN, ACCESS ROAD HAS MORE LIMESTONE |
1870167 | Primary Facility | 2010-02-04 | Follow-up Inspection | No Violations Noted | PRODUCING WELL, OPEN PIT, FENCE IS FALLING DOWN AND PARTIALLY MISSING. ANNULUS IS CLOSED, SITE HAS NOT YET BEEN RESTORED. |
For data sources see[7]