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37-019-00672

Well Details

Well ID: 37-019-00672
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Country: United States
State: Pennsylvania
County: Butler
Municipality: Winfield Township
Operator Name: REDMILL DRILLING
Well Pad ID:
Farm/Lease Name: JOHN W THOMPSON ET AL 10712
License Status: Active
Spud Date: 1/1/1800
Permit Date:
Unconventional Well: N
Configuration: Vertical Well
Latitude: 40.761240
Longitude: -79.777450

For data sources see[1][2][3]

Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
1991 PARKER & PARSLEY DEV LP 333.00 364 0.00 0.00
1992 PARKER & PARSLEY DEV LP 321.00 187 0.00 0.00
1995 PARKER & PARSLEY DEV LP 228.00 209 0.00 0.00
1996 RANGE OPR CO 981.00 365 0.00 0.00
1999 BLX INC 571.00 368 0.00 0.00
2000 BLX INC 676.00 364 0.00 0.00
2001 BLX INC 650.00 334 0.00 0.00
2002 BLX INC 597.59 328 0.00 0.00
2003 0.00 0.00 0.00
2004 BLX INC 881.59 357 0.00 0.00
2005 BLX INC 806.56 364 0.00 0.00
2006 BLX INC 809.00 364 0.00 0.00
2007 BLX INC 856.00 365 0.00 0.00
2008 BLX INC 720.00 365 0.00 0.00
2009 BLX INC 671.00 359 0.00 0.00
2010 BLX INC 619.99 300 0.00 0.00
2011 BLX INC 856.61 304 0.00 0.00
2012 BLX INC 733.57 366 0.00 0.00
2013 REDMILL DRILLING 1,323.72 365 0.00 0.00
2014 REDMILL DRILLING 844.77 269 0.00 0.00
2015 REDMILL DRILLING 926.03 365 0.00 0.00
2016 REDMILL DRILLING 1,049.68 366 0.00 0.00
2017 REDMILL DRILLING 901.60 337 0.00 0.00
2018 REDMILL DRILLING 845.64 273 0.00 0.00

For data sources see[4]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
2739421 Primary Facility 2018-06-06 Routine/Partial Inspection No Violations Noted At the time of inspection, well appeared to be producing. Well integrity appeared to be in good condition, with no signs of any leaks or spills. The well is painted so no corrosion was noticed. The well had a heater and small meter hooked up as well as a drip. There was what appeared to be 5 1/2" inside of 6 5/8" casing. Well was properly labeled. Production was reported in 2017 as 901 mcf for 337 days.

For data sources see[5]

References