X

Track changes made to this page

If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.



Privacy policy
Close this window

powered by ChangeDetection

37-019-01502

Well Details

Well ID: 37-019-01502
Loading map...
Country: United States
State: Pennsylvania
County: Butler
Municipality: Jefferson Township
Operator Name:
Well Pad ID:
Farm/Lease Name: BOYER 1 SAXONY FARMS 4
License Status: Active
Spud Date: 1/1/1800
Permit Date:
Unconventional Well: N
Configuration: Vertical Well
Latitude: 40.751090
Longitude: -79.782010

For data sources see[1][2][3]

Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
2007 0.00 0.00 0.00
2009 0.00 0.00 0.00
2010 HERMAN RIEMER GAS CO 144.00 365 0.00 0.00
2011 HERMAN RIEMER GAS CO 183.00 365 0.00 0.00
2012 HERMAN RIEMER GAS CO 70.00 334 0.00 0.00
2013 HERMAN RIEMER GAS CO 56.00 334 0.00 0.00
2014 HERMAN RIEMER GAS CO 102.00 365 0.00 0.00
2015 HERMAN RIEMER GAS CO 188.00 365 0.00 0.00
2016 HERMAN RIEMER GAS CO 135.00 364 0.00 0.00
2017 HERMAN RIEMER GAS CO 30.00 365 0.00 24.00 2
2018 SME WELL SVC INC 80.00 365 0.00 0.00

For data sources see[4]

Waste Data

Period Waste Type Quantity Disposal Method Waste Facility ID
2012-0 Produced Fluid (in Barrels) 69.00 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE PA0095273
2013-0 Produced Fluid (in Barrels) 32.00 Bbl CENT WASTE TRT FAC NPDES DISCHARGE PA0095273
2014-0 Produced Fluid (in Barrels) 3.00 Bbl CENT WASTE TRT FAC NPDES DISCHARGE PA0101508
2016-0 Produced Fluid (in Barrels) RWC 802 7.00 Bbl CENT WASTE TRT FAC NPDES DISCHARGE PA0101508
2017-0 Drilling Fluid Waste (in Barrels) RWC 803 24.00 Bbl CENT WASTE TRT FAC NPDES DISCHARGE PA0101508
2018-0 Produced Fluid (in Barrels) RWC 802 5.00 Bbl CENT WASTE TRT FAC NPDES DISCHARGE PA0095273

For data sources see[5]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
2675965 Primary Facility 2017-12-21 Routine/Partial Inspection No Violations Noted At the time of inspection, well was producing. The well had what appeared to be 4 7/8" casing and was hooked up to a meter and a drip. The well was properly labeled. Integrity appeared to be in good condition, with no signs of any leaks or spills at the site. The wellhead had some minor rust, but was only superficial. Access to the well was somewhat difficult, with 3 gates to pass through and no access road once past the Snyder Brothers well on the property. Corn was still up at the time.

For data sources see[6]

References