X

Track changes made to this page

If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.



Privacy policy
Close this window

powered by ChangeDetection

37-105-00826

Well Details

Well ID: 37-105-00826
Loading map...
Country: United States
State: Pennsylvania
County: Potter
Municipality: Sharon Township
Operator Name:
Well Pad ID:
Farm/Lease Name: SHERMAN 246
License Status: Active
Spud Date: 1/1/1800
Permit Date:
Unconventional Well: N
Configuration: Vertical Well
Latitude: 41.968465
Longitude: -78.161799

For data sources see[1][2][3]

Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
1994 0.00 0.00 0.00
1995 0.00 0.00 0.00
1996 0.00 0.00 0.00
1997 HOLLIS & KATHRYN NICHOLS 83,333.33 365 0.00 0.00
2000 0.00 0.00 0.00
2001 0.00 0.00 0.00
2002 0.00 0.00 0.00
2003 0.00 0.00 0.00
2004 0.00 0.00 0.00
2005 HOLLIS & KATHRYN NICHOLS 83.00 365 0.00 0.00
2006 0.00 0.00 0.00
2007 HOLLIS & KATHRYN NICHOLS 83.00 365 0.00 0.00
2008 0.00 0.00 0.00
2009 HOLLIS & KATHRYN NICHOLS 624.80 365 0.00 0.00
2010 HOLLIS & KATHRYN NICHOLS 892.17 365 0.17 365 0.17 365
2011 HOLLIS & KATHRYN NICHOLS 903.50 365 0.17 365 0.17 365
2014 HOLLIS & KATHRYN NICHOLS 438.00 365 0.20 365 0.20 365
2015 HOLLIS & KATHRYN NICHOLS 365.00 365 0.20 365 0.20 365
2016 HOLLIS & KATHRYN NICHOLS 269.00 365 0.02 365 0.02 365
2017 HOLLIS & KATHRYN NICHOLS 234.60 365 0.02 365 0.02 365

For data sources see[4]

Waste Data

Period Waste Type Quantity Disposal Method Waste Facility ID
2010-0 Produced Fluid (in Barrels) 1.83 Bbl ROAD SPREADING
2011-0 Produced Fluid (in Barrels) 2.17 Bbl ROAD SPREADING
2014-0 Produced Fluid (in Barrels) 0.20 Bbl ROAD SPREADING
2016-0 Produced Fluid (in Barrels) RWC 802 0.02 Bbl REUSE AT A CONVENTIONAL WELL SITE IN PA
2017-0 Produced Fluid (in Barrels) RWC 802 0.20 Bbl REUSE AT A CONVENTIONAL WELL SITE IN PA

For data sources see[5]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
2802468 Primary Facility 2018-11-14 Routine/Complete Inspection No Violations Noted At the time of this inspection this well was in production. This well is approximately 6"-6 1/2" casing out of the ground reduced to approximately 4"- 4 1/2" then into a threaded fitting of the same size making a wellhead assembly then connecting to a flow line leaving the wellhead going to a production line going into the ground. No violations noted at this inspection.

For data sources see[6]

References