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37-063-36079

Well Details

Well ID: 37-063-36079
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Country: United States
State: Pennsylvania
County: Indiana
Municipality: Canoe Township
Operator Name: ALLIANCE PETROLEUM CO LLC
Well Pad ID:
Farm/Lease Name: BUDD S WINEBERG 7
License Status: Active
Spud Date: 02/15/2009
Permit Date: 6/12/2008
Unconventional Well: N
Configuration: Vertical Well
Latitude: 40.859383
Longitude: -78.980603

For data sources see[1][2][3]

Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
2008 0.00 0.00 0.00
2009 DOMINION EXPLORATION & PROD INC 17,580.34 365 0.00 0.00
2010 CONSOL GAS CO 11,326.00 365 0.00 0.00
2011 0.00 0.00 0.00
2012 CNX GAS CO LLC 6,590.00 366 0.00 0.00
2013 CNX GAS CO LLC 5,454.58 365 0.00 0.00
2014 CNX GAS CO LLC 5,100.11 365 0.00 0.00
2015 CNX GAS CO LLC 3,943.47 365 0.00 0.00
2016 CNX GAS CO LLC 3,547.09 366 0.00 0.00
2017 CNX GAS CO LLC 3,209.74 365 0.00 0.00
2018 CNX GAS CO LLC 2,290.11 365 0.00 0.00

For data sources see[4]

Waste Data

Period Waste Type Quantity Disposal Method Waste Facility ID
2009-0 Brine 159.00 Bbl Brine or Industrial Waste Treatment Plt PA0091472
2009-0 Brine 31.00 Bbl Injection Disposal Well PA101656
2009-0 Fracking Fluid 200.00 Bbl Brine or Industrial Waste Treatment Plt PA0091472
2009-0 Fracking Fluid 1,800.00 Bbl Brine or Industrial Waste Treatment Plt PA0095443
2009-0 Fracking Fluid 440.00 Bbl Other 37-063-36161
2010-0 Produced Fluid (in Barrels) 80.00 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE PA0020346
2011-0 Produced Fluid (in Barrels) 80.00 Bbl CENTRALIZED TREATMENT PLANT FOR RECYCLE PA0095273
2012-0 Produced Fluid (in Barrels) 52.00 Bbl INJECTION DISPOSAL WELL 34-007-22038
2012-0 Produced Fluid (in Barrels) 63.59 Bbl INJECTION DISPOSAL WELL 34-013-20609
2013-0 Produced Fluid (in Barrels) 42.15 Bbl INJECTION DISPOSAL WELL 34-013-20609
2017-0 Produced Fluid (in Barrels) RWC 802 50.00 Bbl SURFACE IMPOUNDMENT 95-7-37312-19

For data sources see[5]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
2385092 Primary Facility 06/24/2015 Administrative/File Review In Compliance with Policy SPILL.
2385103 Primary Facility 06/25/2015 Administrative/File Review In Compliance with Policy Admin inspt in response to inspt record 2385092 for the reported release of less than 5 gallons brine water.Upon receipt of spill report, Dept contacted Richy Vrobel via phone on 6/25/15 at 0735. Mr. Vrobel stated that release resulted from a crack in a patch on tank and that brine leaked onto plywood that tank is positioned on.Tank w/in earthen dike.Mr. Vrobel stated that Spartan will be removing any visibly impacted soils and will conduct sampling to ensure the release is adequately remediated. Mr. Vrobel plans to replace tank.Per Mr. Vrobel, the WT discovered release on 6/24 at 0910 when he observed a wet spot on plywood.Release subsequently reported to SWRO at 0958.
2528683 Primary Facility 2016-10-05 Routine/Complete Inspection No Violations Noted 10/5/2016 - tank, tag.

For data sources see[6]

References