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Well ID: 37-063-36079 | Loading map...
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Country: United States | |
State: Pennsylvania | |
County: Indiana | |
Municipality: Canoe Township | |
Operator Name: ALLIANCE PETROLEUM CO LLC | |
Well Pad ID: | |
Farm/Lease Name: BUDD S WINEBERG 7 | |
License Status: Active | |
Spud Date: 02/15/2009 | |
Permit Date: 6/12/2008 | |
Unconventional Well: N | |
Configuration: Vertical Well | |
Latitude: 40.859383 | |
Longitude: -78.980603 |
Period | Operator Name | Gas Quantity (mcf) | Gas Production Days | Oil Quantity (bbl) | Oil Production Days | Water Quantity (bbl) | Water Production Days |
---|---|---|---|---|---|---|---|
2008 | 0.00 | 0.00 | 0.00 | ||||
2009 | DOMINION EXPLORATION & PROD INC | 17,580.34 | 365 | 0.00 | 0.00 | ||
2010 | CONSOL GAS CO | 11,326.00 | 365 | 0.00 | 0.00 | ||
2011 | 0.00 | 0.00 | 0.00 | ||||
2012 | CNX GAS CO LLC | 6,590.00 | 366 | 0.00 | 0.00 | ||
2013 | CNX GAS CO LLC | 5,454.58 | 365 | 0.00 | 0.00 | ||
2014 | CNX GAS CO LLC | 5,100.11 | 365 | 0.00 | 0.00 | ||
2015 | CNX GAS CO LLC | 3,943.47 | 365 | 0.00 | 0.00 | ||
2016 | CNX GAS CO LLC | 3,547.09 | 366 | 0.00 | 0.00 | ||
2017 | CNX GAS CO LLC | 3,209.74 | 365 | 0.00 | 0.00 | ||
2018 | CNX GAS CO LLC | 2,290.11 | 365 | 0.00 | 0.00 |
For data sources see[4]
Period | Waste Type | Quantity | Disposal Method | Waste Facility ID |
---|---|---|---|---|
2009-0 | Brine | 159.00 Bbl | Brine or Industrial Waste Treatment Plt | PA0091472 |
2009-0 | Brine | 31.00 Bbl | Injection Disposal Well | PA101656 |
2009-0 | Fracking Fluid | 200.00 Bbl | Brine or Industrial Waste Treatment Plt | PA0091472 |
2009-0 | Fracking Fluid | 1,800.00 Bbl | Brine or Industrial Waste Treatment Plt | PA0095443 |
2009-0 | Fracking Fluid | 440.00 Bbl | Other | 37-063-36161 |
2010-0 | Produced Fluid (in Barrels) | 80.00 Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | PA0020346 |
2011-0 | Produced Fluid (in Barrels) | 80.00 Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | PA0095273 |
2012-0 | Produced Fluid (in Barrels) | 52.00 Bbl | INJECTION DISPOSAL WELL | 34-007-22038 |
2012-0 | Produced Fluid (in Barrels) | 63.59 Bbl | INJECTION DISPOSAL WELL | 34-013-20609 |
2013-0 | Produced Fluid (in Barrels) | 42.15 Bbl | INJECTION DISPOSAL WELL | 34-013-20609 |
2017-0 | Produced Fluid (in Barrels) RWC 802 | 50.00 Bbl | SURFACE IMPOUNDMENT | 95-7-37312-19 |
For data sources see[5]
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
2385092 | Primary Facility | 06/24/2015 | Administrative/File Review | In Compliance with Policy | SPILL. |
2385103 | Primary Facility | 06/25/2015 | Administrative/File Review | In Compliance with Policy | Admin inspt in response to inspt record 2385092 for the reported release of less than 5 gallons brine water.Upon receipt of spill report, Dept contacted Richy Vrobel via phone on 6/25/15 at 0735. Mr. Vrobel stated that release resulted from a crack in a patch on tank and that brine leaked onto plywood that tank is positioned on.Tank w/in earthen dike.Mr. Vrobel stated that Spartan will be removing any visibly impacted soils and will conduct sampling to ensure the release is adequately remediated. Mr. Vrobel plans to replace tank.Per Mr. Vrobel, the WT discovered release on 6/24 at 0910 when he observed a wet spot on plywood.Release subsequently reported to SWRO at 0958. |
2528683 | Primary Facility | 2016-10-05 | Routine/Complete Inspection | No Violations Noted | 10/5/2016 - tank, tag. |
For data sources see[6]