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37-125-01279

Well Details

Well ID: 37-125-01279
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Country: United States
State: Pennsylvania
County: Washington
Municipality: Blaine Township
Operator Name: DALLAS ENERGY LLC
Well Pad ID:
Farm/Lease Name: MEHAFFEY E 1
License Status: Plugged OG Well
Spud Date: 1/1/1800
Permit Date:
Unconventional Well: N
Configuration: Vertical Well
Latitude: 40.190033
Longitude: -80.367966

For data sources see[1][2][3]

Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
1993 0.00 0.00 0.00
1996 0.00 0.00 0.00
1997 0.00 0.00 0.00
1998 0.00 0.00 0.00
1999 0.00 0.00 0.00
2000 0.00 0.00 0.00
2001 0.00 0.00 0.00
2002 0.00 0.00 0.00
2003 0.00 0.00 0.00
2005 0.00 0.00 0.00
2006 0.00 0.00 0.00
2007 0.00 0.00 0.00
2008 0.00 0.00 0.00
2010 0.00 0.00 0.00
2011 0.00 0.00 0.00
2012 0.00 0.00 0.00
2013 0.00 0.00 0.00
2014 0.00 0.00 0.00
2015 0.00 0.00 0.00
2016 0.00 0.00 0.00

For data sources see[4]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
2488911 Primary Facility 2016-05-16 Plugging(Includes Plugged/Mined Through) In Compliance with Schedule ConServ is moving equipment in, rig is on location & ready to rig up.
2488915 Primary Facility 2016-05-19 Plugging(Includes Plugged/Mined Through) In Compliance with Schedule ConServ TIH w/ bond log, set down on 1st cement plug TOC @1730 feet. Log 4 1/2" casing, packer @1634-38 feet. Free pipe to surface.
2488922 Primary Facility 2016-05-23 Plugging(Includes Plugged/Mined Through) In Compliance with Schedule ConServ running cement string in hole. Had to remove some of concrete slab around wellhead and reset liner.
2488923 Primary Facility 2016-05-24 Plugging(Includes Plugged/Mined Through) In Compliance with Schedule ConServ tagged TOC plug @ 1225, cut 4 1/2" casing 1185', pulled free.
2488927 Primary Facility 2016-05-26 Plugging(Includes Plugged/Mined Through) In Compliance with Schedule ConServ cemented well to surface & rigged down.
2488931 Primary Facility 2016-05-27 Plugging(Includes Plugged/Mined Through) In Compliance with Schedule ConServ rough graded location after equipment moved. Will bury well marker.
773492 Primary Facility 05/28/1997 Routine/Complete Inspection No Violations Noted MEASURED FLUID LEVEL WITH EPA

For data sources see[5]

References