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37-125-01661

Well Details

Well ID: 37-125-01661
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Country: United States
State: Pennsylvania
County: Washington
Municipality: Blaine Township
Operator Name: DALLAS ENERGY LLC
Well Pad ID:
Farm/Lease Name: A.M. HEWITT 1
License Status: Plugged OG Well
Spud Date: 1/1/1800
Permit Date:
Unconventional Well: N
Configuration: Vertical Well
Latitude: 40.152114
Longitude: -80.409047

For data sources see[1][2][3]

Production Data

Period Operator Name Gas Quantity (mcf) Gas Production Days Oil Quantity (bbl) Oil Production Days Water Quantity (bbl) Water Production Days
1991 PENNZOIL PROD CO 1,482.00 365 0.00 0.00
1993 PENNZOIL PROD CO 753.00 365 0.00 0.00
1996 PENNZOIL PROD CO 668.00 365 0.00 0.00
1997 PENNZOIL PROD CO 201.00 365 0.00 0.00
1998 PENNZOIL PROD CO 1,307.00 365 0.00 0.00
1999 0.00 0.00 0.00
2000 0.00 0.00 0.00
2001 EAST RESOURCES INC 79.40 365 0.00 0.00
2002 0.00 0.00 0.00
2003 0.00 0.00 0.00
2005 0.00 0.00 0.00
2006 0.00 0.00 0.00
2007 0.00 0.00 0.00
2008 0.00 0.00 0.00
2010 0.00 0.00 0.00
2011 0.00 0.00 0.00
2012 0.00 0.00 0.00
2013 0.00 0.00 0.00
2014 0.00 0.00 0.00
2015 0.00 0.00 0.00
2016 0.00 0.00 0.00
2017 0.00 0.00 0.00

For data sources see[4]

Inspection Data

Inspections Performed

Inspection ID Inspection Category Inspection Date Inspection Type Inspection Result Inspection Comments
2644292 Primary Facility 2017-09-11 Plugging(Includes Plugged/Mined Through) In Compliance with Policy ConServ had spotted bottom hole plug, tagged with wireline @ 1855'. Bottom of 6 5/8" casing (wireline) @ 1820'. Drillers log listed btm @ 1740'.
2649252 Primary Facility 2017-09-12 Plugging(Includes Plugged/Mined Through) In Compliance with Policy ConServ perfing 6 5/8" casing to surface, currently perfing @ 900'. Will pump next cement plug when finished.
2649308 Primary Facility 2017-09-13 Plugging(Includes Plugged/Mined Through) In Compliance with Policy ConServ tagged TOC plug @ 1668'. Pumped next plug, calculated to be 1000', will tag later today. Plugs have not been circulating to surface because the perfs @ _500' have been drinking fluid.

For data sources see[5]

References