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Well ID: 37-115-21609 | ![]() Sorry, we have no imagery here. Sorry, we have no imagery here. Sorry, we have no imagery here. ![]() |
Country: United States | |
State: Pennsylvania | |
County: Susquehanna | |
Municipality: Harford Township | |
Operator Name: CHIEF OIL & GAS LLC | |
Well Pad ID: 150754 | |
Farm/Lease Name: HERBERT UNIT 1H | |
License Status: Active | |
Spud Date: 11/25/2014 | |
Permit Date: 1/28/2014 | |
Unconventional Well: Y | |
Configuration: Horizontal Well | |
Latitude: 41.727850 | |
Longitude: -75.687433 |
Period | Operator Name | Gas Quantity (mcf) | Gas Production Days | Oil Quantity (bbl) | Oil Production Days | Water Quantity (bbl) | Water Production Days |
---|---|---|---|---|---|---|---|
2014 | CHIEF OIL & GAS LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2015 | CHIEF OIL & GAS LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2016 | CHIEF OIL & GAS LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2017 | CHIEF OIL & GAS LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
2019 | CHIEF OIL & GAS LLC | 0.00 | 0 | 0.00 | 0 | 0.00 | 0 |
For data sources see[4]
Period | Waste Type | Quantity | Disposal Method | Waste Facility ID |
---|---|---|---|---|
2014-2 | Drill Cuttings (in Tons) | 512.03 Tons | LANDFILL | 100933 |
2014-2 | Drilling Fluid Waste (in Barrels) | 1,306.40 Bbl | RESIDUAL WASTE PROC FAC (GENERAL PERMIT) | WMGR123 |
2018-05 | Drill Cuttings (in Tons) RWC 810 | 365.51 Tons | LANDFILL | 100933 |
2018-05 | Drilling Fluid Waste (in Barrels) RWC 803 | 821.72 Bbl | RESIDUAL WASTE PROCESSING FACILITY | WMGR123NC010 |
2018-06 | Drill Cuttings (in Tons) RWC 810 | 95.11 Tons | LANDFILL | 301358 |
For data sources see[5]
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
2268038 | Primary Facility | 05/01/2014 | Preoperation Inspection | No Violations Noted | The Department was on site at the Chief Herbert Well Pad to conduct a Preoperational Inspection. Inspection conducted with Frank Hoehle and Merle Wade, construction inspector. The well permit that has been issued for this pad is the 1H (115-21609). All perimeter BMP’s in place to include red lined additions. Entrance has not been black topped yet. P7 cross culvert has not been installed. Pipe is on-site and will be installed shortly. Pad slopes are approximately 10% complete. Pad is 75% complete. No violations noted. |
2328442 | Primary Facility | 12/08/2014 | Drilling/Alteration | No Violations Noted | |
2406791 | Primary Facility | 09/14/2015 | Routine/Complete Inspection | No Violations Noted | |
2469591 | Primary Facility | 2016-03-30 | Routine/Complete Inspection | No Violations Noted | On 3/30/16, the Department conducted an inspection of the Chief Herbert Well Pad. Only one well has been drilled on this pad, the Herbert 1H 9115-21609). A review of the Well Record revealed that the production string has yet to be drilled. The conductor (20”), the surface string (13 3/8”), and the intermediate string (9 5/8”) have been drilled and set. Date well completed was 12/12/2014. The cellar is approximately 1/3 full of water, with no bubbling present. Pad and slopes stable with good vegetation. No violations noted. |
2483830 | Primary Facility | 2016-05-13 | Routine/Complete Inspection | No Violations Noted | |
2555313 | Primary Facility | 2017-01-25 | Routine/Complete Inspection | No Violations Noted | At time of inspection, arrived on site at 14:10p.m., the cellar was about a quarter full of water and ice with no bubbling noticed. There were no lines going to or from the well and there was a night cap on the well, all the valves on the well were closed. There were no tanks and production units on site. The well was granted inactive status on 6/24/2016, only the vertical section of the well has been drilled to a depth of 6448'. I took a walk around the location and there were no obvious concerns noticed.
I left the site at 14:30p.m. |
2643493 | Primary Facility | 2017-10-03 | Routine/Complete Inspection | No Violations Noted | At time of inspection.
The well was granted inactive status on 6/24/16. The top-hole section of the well was drilled to a depth of 6448'. There were no lines going to or from the well. All the valves were closed and there was a TA cap on top of the well. There were no tanks or production units on the site. I took a walk around the location and there were no obvious concerns noticed. There were no violations noted. |
2687760 | Primary Facility | 2018-01-22 | Routine/Complete Inspection | No Violations Noted | Today's inspection was conducted as a routine inspection. Site snow covered. Plowing has occurred since last snow fall. No E&S issues observed. No violations noted. |
2764055 | Primary Facility | 2018-08-09 | Routine/Complete Inspection | No Violations Noted | Today's inspection was conducted as a routine inspection. No E&S issues were observed. No violations noted. |
2831887 | Primary Facility | 2019-01-25 | Follow-up Inspection | No Violations Noted | Today's inspection was conducted as a follow-up inspection. This inspection found that the violations noted in the Department inspection conducted on 10/22/18 and 11/30/18 and documented in Inspection Record #'s 2796240 and 2808752 respectively have been corrected. Drilling has been completed on the 1H and 4H. No stimulation has occurred yet. Overall the site has good stabilization. No E&S issues identified. No violations noted. |
For data sources see[6]