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Well ID: 37-039-21281 | Loading map...
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Country: United States | |
State: Pennsylvania | |
County: Crawford | |
Municipality: Spring Township | |
Operator Name: B & R RESOURCES LLC | |
Well Pad ID: | |
Farm/Lease Name: CARL S & BARBARA H TIMKO 2 | |
License Status: Active | |
Spud Date: 08/14/1981 | |
Permit Date: 6/29/1981 | |
Unconventional Well: N | |
Configuration: Vertical Well | |
Latitude: 41.822087 | |
Longitude: -80.359703 |
Period | Operator Name | Gas Quantity (mcf) | Gas Production Days | Oil Quantity (bbl) | Oil Production Days | Water Quantity (bbl) | Water Production Days |
---|---|---|---|---|---|---|---|
1982 | TIMBERLINE ENERGY INC | 9,389.51 | 0 | 0.00 | 0.00 | ||
1985 | TIMBERLINE ENERGY INC | 3,691.00 | 0 | 0.00 | 0.00 | ||
1986 | TIMBERLINE ENERGY INC | 746 | 258 | 146 | 258 | 0.00 | |
1987 | TIMBERLINE ENERGY INC | 118 | 242 | 242 | 0 | 0.00 | |
1988 | TIMBERLINE ENERGY INC | 667 | 365 | 84 | 365 | 0.00 | |
1989 | TIMBERLINE ENERGY INC | 470 | 365 | 41 | 365 | 0.00 | |
1990 | TIMBERLINE ENERGY INC | 150.00 | 365 | 0.00 | 0.00 | ||
1991 | SEQUOIA MGMT CO INC | 527.00 | 365 | 79.00 | 365 | 0.00 | |
1996 | EXCO RESOURCES PA INC | 0.00 | 32.21 | 365 | 0.00 | ||
1997 | 0.00 | 0.00 | 0.00 | ||||
1998 | 0.00 | 0.00 | 0.00 | ||||
1999 | 0.00 | 0.00 | 0.00 | ||||
2000 | 0.00 | 0.00 | 0.00 | ||||
2001 | EXCO RESOURCES PA INC | 225.00 | 244 | 172.00 | 244 | 0.00 | |
2005 | DYLAN RES LLC | 83.00 | 365 | 0.00 | 0.00 | ||
2006 | DYLAN RES LLC | 83.00 | 365 | 0.00 | 0.00 | ||
2007 | 0.00 | 0.00 | 0.00 | ||||
2008 | DYLAN RES LLC | 41.50 | 365 | 0.00 | 0.00 | ||
2010 | 0.00 | 0.00 | 0.00 | ||||
2011 | 0.00 | 0.00 | 0.00 | ||||
2012 | 0.00 | 0.00 | 0.00 | ||||
2013 | 0.00 | 0.00 | 0.00 | ||||
2014 | 0.00 | 0.00 | 0.00 |
For data sources see[4]
Period | Waste Type | Quantity | Disposal Method | Waste Facility ID |
---|---|---|---|---|
1991-A00 | Brine | 141.00 Bbl | ||
1996-A00 | Brine | 272.50 Bbl | Injection Disposal Well |
For data sources see[5]
Inspection ID | Inspection Category | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|---|
2263375 | Primary Facility | 03/19/2014 | Routine/Complete Inspection | Violation(s) Noted | |
2369135 | Primary Facility | 05/05/2015 | Routine/Complete Inspection | Outstanding Violations - No Viols Req'd | |
2653321 | Primary Facility | 2017-10-27 | Compliance Evaluation | Violation(s) Noted | Inspected location, well is equipped with 8 5/8's surface casing, 4 1/2 production casing and is swedged down to 2" with a valve, well has no equipment for production nor is is hooked to any line, well is still abandon, appears that there has been brine coming out of annulus onto ground, dead vegetation around wellhead. |
375161 | Primary Facility | 1993-11-17 | Routine/Complete Inspection | No Violations Noted |
Inspection ID | Violation ID | Violation Date | Date Resolved | Violation Code | Violation Type | Violation Comments |
---|---|---|---|---|---|---|
2263375 | 693459 | 03/19/2014 | OGA 3220(A) - Failure to plug the well upon abandoning it. | Environmental Health & Safety | No production equipment at wellsite. Wellhead not connected to any piping. | |
2653321 | 800261 | 2017-10-27 | OGA3259(1) | Environmental Health & Safety |
For data sources see[6]