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Well ID: 34-105-23445 | Loading map...
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Country: United States | |
State: Ohio | |
County: Meigs | |
Municipality: Chester | |
Operator Name: MOUNTAINEER STATE OPERATIONS L | |
Well Pad ID: | |
Farm/Lease Name: DAMEWOOD OWEN | |
License Status: Producing | |
License Date: 1985-12-13 | |
Spud Date: 1986-04-03 | |
Spud Drilling Contractor: | |
Final Drill Date: 1986-04-09 | |
Well Total Depth: 3370 ft | |
Configuration: Vertical | |
Latitude: 39.121342647 | |
Longitude: -81.85779586 |
For data sources see[1]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 2425 | 3238 | 43 |
For data sources see[1]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
000PL10610 | Preliminary Restoration | No Violations | Preliminary Restoration done information from Data Point | |
0816992307 | 2018-08-08 | Production Wells | No Violations | The gas leak was stopped, violation is resolved. |
1101958256 | 2013-09-25 | Production Wells | No Violations | Valve on production open. Tank battery is 100 barrel steel tank. |
1533743674 | 2018-08-08 | Production Wells | Violations Noted | I called Ronnie the well tender for Carl E Smith and explained that the 4.5 inch casing was leaking around the worm gear clamp. Ronnie said he told John Kent about the issue a couple months ago. Ronnie said he would be on his way out. I then tried to call John Kent and his phone went straight to voicemail. I then called the number listed in RBDMS. The number was a Dallas, TX number and it was the voicemail of Patty Murphy. I called this number approximately 10 times in a row. Patty finally answered the phone and I went over 6 different wells and the violations and explained that one of them is already a Chiefs Order and the rest are headed that way. She explained she would get right on it. I finished the phone call explaining that I was at a well with a gas leak in the 4.5 inch and was waiting on Ronnie because he answered the phone and was on his way. I explained that if he couldnt get the leak to stop I would have to notify the Emergency Response group. When Ronnie showed up he was able to get the leak stopped so this violation is now closed. |
1600285580 | 2010-08-11 | Production Wells | No Violations | Identification on production equipment. New chart in meter was changed on 7-30-10. Well is connected to production line. Valves are open. Wellsite has been mowed recently. 100 bbl steel tank has dike around it. Dike needs drained. I called Tom Stone and he is having the water truck come clean out the dike. |
1737043343 | 2017-03-24 | Production Wells | No Violations | Well is a producing gas well with an active chart, while I was there I could hear it selling. Well has chart, drip, meter and a 100 barrel steel tank. The 4.5 inch diameter pipe in the 7.1 inch diameter casing head has a piece of rubber around it with 2 worm gear clamps to stop a leak. The flow line from the tubing has a clamp on it at ground level to prevent the pipe from leaking. These are just quick cheap fixes and will eventually fail. These will need fixed correctly to prevent future emergency situations. Identification was faded and rusted. |
1970681858 | 2005-03-04 | Production Wells | No Violations | An inspection found no violations. |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1533743674 | US-OH-114745 | 2018-08-17 | 9-9-05(A)1 | Well insufficiently equipped to prevent escape of oil and gas |
1533743674 | US-OH-114746 | 2018-08-17 | 9-9-05(A)8 | Equipment pressure rated below operating pressure |
For data sources see[1]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
Not Treated | 0 | 70000 | 0 | SCFM | ||
N2 | 0 | 1500 Mscf | 0 | |||
ACID | 0 | 500 Gal | 0 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1985-12-13 | 248 SMITH CARL E PETROL INC GeoDate 12/13/85 |
Oil and Gas | 1985-12-13 | Issued Date 12/13/85 Expired Date 12/13/86 Acres 0074630 Tool Type RTAF Proposed Formation BER/OH SHALE Proposed Depth 03370 Proposed Drill Depth 03370 |
Original Spud | 1986-04-03 | |
Completed | 1986-04-09 | |
Reached Total Depth | 1986-04-09 | |
Completion Report Received | 1986-06-16 | |
Construction Permit Expires | 1986-12-13 | |
Change of Owner | 2019-03-12 | Operator changed from 248, CARL E SMITH PETROLEUM INC to 8473, MOUNTAINEER STATE OPERATIONS LLC |
Record Last Modified | 2019-03-12 |
For data sources see[1]