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Well ID: 34-111-22673 | Loading map...
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Country: United States | |
State: Ohio | |
County: Monroe | |
Municipality: Franklin Township | |
Operator Name: RACK RIDGE LLC | |
Well Pad ID: | |
Farm/Lease Name: FREDRICK | |
License Status: Final Restoration | |
License Date: 2015-11-09 | |
Spud Date: | |
Spud Drilling Contractor: | |
Final Drill Date: | |
Well Total Depth: | |
Configuration: Vertical | |
Latitude: 39.710324691 | |
Longitude: -81.30666377 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1981-11-18 | 2947 REUSSER LYNN & HERMAN GeoDate 11/18/81 |
Change of Owner | 2002-02-26 | Operator changed from 2947, REUSSER LYNN & HERMAN to 6283, TENNANT LARRY P & BARBARA J |
Change of Owner | 2002-07-01 | Operator changed from 6283, TENNANT LARRY P & BARBARA J to 7239, BOYD |
APP | 2015-06-24 | Proposed Formations:BEREA, Issued Date:6/24/2015, Expired Date:6/23/2017 12:00:00 PM, Drilling unit acres:10, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2015-10-06 | PERMIT EXPIRED. |
Record Last Modified | 2017-02-10 | PERMIT EXPIRED. |
Construction Permit Expires | 2017-06-23 | PERMIT EXPIRED. |
For data sources see[2]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
2008 | RACK RIDGE LLC | 0 | 17 | 365 |
2009 | RACK RIDGE LLC | 64 | 0 | 365 |
2010 | RACK RIDGE LLC | 9 | 0 | 50 |
2011 | RACK RIDGE LLC | 70 | 5 | 365 |
2012 | RACK RIDGE LLC | 47 | 0 | 366 |
2013 | RACK RIDGE LLC | 45 | 0 | 200 |
2015 | RACK RIDGE LLC | 47 | 0 | 120 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
2008 | RACK RIDGE LLC | Brine | 26 | 365 |
2009 | RACK RIDGE LLC | Brine | 0 | 365 |
2010 | RACK RIDGE LLC | Brine | 0 | 50 |
2011 | RACK RIDGE LLC | Brine | 20 | 365 |
2012 | RACK RIDGE LLC | Brine | 0 | 366 |
2013 | RACK RIDGE LLC | Brine | 0 | 200 |
2015 | RACK RIDGE LLC | Brine | 0 | 120 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
0018092733 | 2010-08-10 | Production Wells | No Violations | On day of inspection Boyd and I and Bret Farnsworth went in to site. There was 90%vegetation.Well is going to be a swab well.Well is in compliance.NOV is resolved. |
0058842242 | 2014-09-29 | Administrative Inspection | No Violations | Administrative inspection to document the unresolved compliance notice, no contact has been received by Harry Boyd with Rack Ridge concerning the unresolved violation. |
0153713132 | 2009-04-09 | Production Wells | No Violations | |
0210532133 | 2014-06-26 | Production Wells | No Violations | Compliance notice 2001769233 follow up inspection found the production valve in the closed position and the 1.250 flow line cut in half near the well head. The well is still incapable of production in its current state and has a unresolved compliance notice issued on it requiring plugging and abandonment. |
1130397897 | 2015-10-02 | Plug / Plug Back | No Violations | I am onsite to witness the plugging operations. 1.5 tubing was already set at a depth of 1293 by Robert Armstrongs service rig. Cemenco circulated a 15 sack class A plug from 1293 to 993. The service rig pulled the 1.5 tubing out of the well. Jet Wireline Services utilized a collar buster shot at 749 to cut the 3 drill pipe (production casing). Circulation could not be established. The service rig then pulled up to 417 where circulation could be established and circulated cement up to 200. Casing was then pulled up to 200 and cement was circulated to surface. |
1255054457 | 2009-10-08 | Production Wells | No Violations | WELL IS SUPPLIED WITH 3HYDRIL PIPE.WELL MAKES LITTLE GAS.NO DOMESTIC HOOKUP.ID INPLACE.THERE IS 90%+VEGATATION.NO PRODUCTION HAS BEEN TURNED IN TO STATE. |
1259001160 | 2009-11-09 | Production Wells | Violations Noted | On day of inspection found that well was shut in and Rack Ridge has not been filing the production reports to the State. Plug or Produce. Failure to comply may result in bond forfeiture. File production reports with the State. |
1281687531 | 2008-12-05 | Production Wells | Violations Noted | WELL IS SHUT IN AND HAS 3HYDRIL IN IT.WELL IS PERFERATED THROUGH THE DRILL PIPE AND MAKES GAS.WELL NEEDS ID. |
1443192647 | 2015-09-25 | Plug / Plug Back | No Violations | On site inspection to witness the 1,292of 1.5 tubing ran into the well inside the 3 production casing. Company records show JET Wireline Service logged the well on 08-13-2008 with a recorded total depth of 1,273 and top of cement on the annular side of the 3 @ 992. |
1444149722 | 2015-10-06 | Administrative Inspection | No Violations | Compliance notice 2001769233 follow up inspection to document the resolution of the violation. The well was plugged on 10/02/2015. |
1796101288 | 2009-04-09 | Production Wells | No Violations | WELL IS CAPABLE WITH GAS LINE TIED IN TO COMMERCIAL PRODUCTION.WELL HAS 3HYDRILL AND NEEDS SWABBED OUT ONCE A YEAR.WELL IS COMPLIANT. |
1863632556 | 2015-10-06 | Plug / Plug Back | No Violations | I met Robert Armstrong on location and verified the cement stayed at surface so he could cut the casing off and begin the reclamation. The cement top was visible approximately four feet from surface. Mr. Armstrong was instructed to reclaim the site in accordance with 1509.072(B). |
1867428980 | 2014-06-26 | Production Wells | No Violations | I am accompanied by Oil & Gas Inspector Bill Stolarik. My inspection finds the well is shut in and the gas line leading from the well appears to be parted. |
1946435807 | 2015-11-09 | Final Restoration | No Violations | Final Restoration status check inspection found the wells site meets ORC 1509.072. The equipment has been removed and the location reclaimed, the landowner and well owner Harry Boyd will continue to use the roadways to access the property and remaining existing wells. |
2001769233 | 2014-03-26 | Production Wells | Violations Noted | Status check inspection found the following equipment present at the well head-3.500 high drill tubing with a reducing swage down to a 2 valve in the closed position with a 2 flow line present and proper well identification posted. Database records show the reported production to be below the minimum standard of 100 mcf since 2008. Instructions are as follows -plug the said well within 180 days- ODNR contact-Monroe Co inspector Bill Stolarik 740-507-6592. |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1259001160 | US-OH-106973 | 2009-11-23 | Well shall be plugged | |
1259001160 | US-OH-106974 | 2009-11-23 | Urban - failure to meet tank battery setbacks from mandatory pooled property | |
1281687531 | US-OH-107827 | 2008-12-08 | Failure to legibly identify well | |
1281687531 | US-OH-107828 | 2008-12-08 | Well shall be plugged | |
2001769233 | US-OH-120317 | 2015-11-23 | Well shall be plugged |
For data sources see[7]